Category Archives: Projects

20230220 – Accessory Building Project Update

[ This post is mostly photos with captions. ]

MONDAY 20 February

The barn as seen from the southeast.  The trench with the conduit for the service conductors still needs to be completely filled in.  The green(ish) bags along the edge of the driveway are top soil.

Although we were still involved in final packing decisions for our cruise, it was a reasonably nice day, weather-wise, so I took a few more photos of the new barn doors and the daytime light levels in the barn with the doors closed.  We zoomed with Paul and Nancy at 5:30 PM, to compare notes and see if there was anything any of us had forgotten to pack for our upcoming cruise.

 

The inside front half of the barn, with the doors closed, as seen from the landing at the top of the stairs to the storeroom.  The 12,000 Lumen ceiling light and the light over the entry door are both turned on. The bottom seals on the roll-up doors are slightly off the concrete to allow them to relax and expand.

 

The large/west RV bay as seen from near its roll-up door.  All of the doors are closed.  The 12,000 Lumen ceiling light and the light over the entry door are both turned on.

 

The small/east RV bay as seen from near the entry door.  All of the doors are closed.  The 12,000 Lumen ceiling light and the light over the entry door are both turned on.

 

 

 

 

 

 

 

 

 

 

 

The Barrina 2’ integrated LED strip light under the stairs is turned on.  In general, the light levels were adequate with this minimal amount of lighting supplementing the daylight coming in through the windows and sun tunnels.  With RVs in the two bays, however, additional lighting will be needed.

 

 

 

 

 

 

 

 

 

 

 

202302(16-18) – Accessory Building Project Update

[ This post is mostly photos with captions. ]

THURSDAY 16 February

This is how the roll-up doors were packed for shipping.  They were made in Missouri and shipped to West Virginia by mistake.  Dan (from Everlast Doors & More) chose to drive to West Virginia to get them, rather than delay the installation by some unknown number of additional weeks.

It was a BIG DAY today.  Dan, from Everlast Doors & More, showed up with the two large roll-up doors for the barn!  Chuck (the builder) arrived shortly thereafter to help Dan with the installation by operating the Pettibone Telehandler.  The telehandler was used to unload the crates from Dan’s trailer and then to lift each door into position while Dan secured the mounts on each end from a ladder.

 

 

 

 

 

One of the doors has been removed from the trailer by the telehandler and is being moved into the large/west RV bay.

 

One of the roll-up doors positioned in the large/west RV bay, ready to be uncrated.

 

 

 

 

 

 

 

 

The chain drive box for a roll-up door.

 

 

 

 

 

 

 

 

 

 

The main ring gear on one end of a roll-up door tube.

 

 

 

 

 

 

A shaft support and tensioner on the opposite end of the roller tube from the ring gear.

 

 

 

 

 

 

 

A chain drive box mounted on the ring gear end of the roller tube.

 

 

 

 

 

 

 

 

 

 

The other roll-up door being lifted into place.  It is supported by a small section of the original shipping crate to allow the telehandler forks to get under it, and is strapped down to hold it in place.

 

 

 

 

 

 

 

 

 

The small/east RV bay roll-up door (on the left in this photo) is installed.  The large/west RV bay roll-up door is being lifted into position with the telehandler.  The telehandler weighs 28,000 pounds, so Chuck (the builder/operator) kept it off of the poured concrete at all times.

 

Dan is securing one end of the large/west RV bay roll-up door to the vertical steel support and bracket.

 

 

 

 

 

 

 

 

FRIDAY 17 February

The weather forecast for today was for cold temperatures and light icing.  I texted Dan early and suggested that he not finish the doors today.  He appreciated that, and said he would be out around noon tomorrow to continue the installation.

 

SATURDAY 18 February

Dan works on the chain drive end of the small/east RV bay roll-up door.

Good to his word, Dan was back around noon and put in a long afternoon finishing the installation of the two big roll-up doors.  He did not like the weather-stripping that came with the doors, and wanted to come back late next week with a different product and finish up.  He would also finish installing the lag screws for the side channels at that time.  (As it turned out, the weather stripping did not get installed until mid-late March, but that’s for another/later post.)

 

 

 

 

 

 

Dan checks the small/east RV bay roll-up door for proper operation.

 

The large/west RV bay roll-up door in the closed position.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

The barn finally has all of its doors and is now closed in and can be secured.

 

20230215 – Accessory Building Project Update

WEDNESDAY 15 February

The Hyperlite light fixture is the small gray object top center in the photo.

The Motor Cities Electric Utilities crew was here today to replace the utility pole in the SE corner of our property, but that work was not directly related to the barn project, and I covered it in a general post for February 01 – 21.

The other thing that happened today was I bought an appliance cord (pigtail) and wired up the Hyperlite outdoor LED fixture that I recently bought on Amazon.  This is a 40W, 5,200 Lumen, 5000K integrated LED light fixture.  I mounted it above the entry door inside the barn so I could test its intensity and beam spread.  Besides possible use on the outside of the barn, I was planning to use these fixtures for interior lighting along the outside edges of the RV bays.  They come in 60W and 100W versions, but I will use more of the lower wattage / lower lumen units for better, more even coverage.

 

The Hyperlite light fixture has two parts with a hinge design that allows them to be separated for installation.  This is the base unit of the light fixture mounted to a framing member above the entry door.  The WAGO lever-nut connectors have been installed on the pigtail power cord.  It has the weathertight seal that goes between the two parts.  The lamp head is adjustable from 0 (straight down) to 90 degrees (straight out) and contains the electronic module and wires for connecting to the incoming power.  The base unit has five (5) access holes with weathertight plugs for getting power into and out of the box.  It has provision for mounting screws in the back and a built-in bubble level to aid in the installation.  It’s listed on Amazon as a commercial unit, and the construction appears to merit that description.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

The lamp head has been set onto the hinge pins of the base and the wires connected via the WAGO lever-nuts.

 

 

 

 

 

 

 

 

I finally got a chance to test the 12,000 Lumen light fixture at night.  It made a LOT of light!

 

One of the Barrina 2’ LED strip lights lit up the area under the stairs quite nicely.

In addition to the 12,000 Lumen ceiling light fixture, and the light over the entry door, I bought two Barrina 2’ LED strip lights from Amazon to test.  These are 20W, 2,500 Lumen, 5000K integrated LED fixtures that I plan to use for the ceiling lighting in the shop and storeroom.  (They also have a 4’, 40W, 5,000 Lumen version.)  For testing purposes , however, I mounted one of these under the stairs/landing, where it will likely remain.  They came with plug-in power cords, so I used one to plug the fixture into an extension cord with multiple receptacles.  They also come with pigtail cables for direct wiring (via an outlet box) and 4’ connector cables, that allow them to be connected end-to-end, only requiring one power feed to an entire string of fixtures.

 

The is the large/west RV bay at night.  With nothing in the bay, the 12,000 Lumen ceiling fixture by the entry door lights up the entire space surprisingly well.  The two strip lights under the stairs are also on, and the Hyperlite light over the entry door is probably also on.

 

 

 

 

 

 

 

 

 

 

 

This photo was taken from the right/east RV bay door.  The main light source is the Hyperlite fixture on the wall above the entry door.  The light under the stairs is from one of the Barrina 2’ LED strip lights.

 

202302(07-10) – Accessory Building Project Update

Winter was still with us, and seemed unable to make up its mind as to whether it would hang around for a while or depart the Great Lakes Region earlier than usual.  Although we finally had electrical power to the barn, which was a huge deal, the big roll-up doors were not yet available for installation, which meant the building was not yet truly weather tight.

 

TUESDAY 07

As I mentioned in the regular post for February 01 – 21, we picked up the 14’ Werner 2-sided step ladder from Lowe’s a few days ago.

The new 14’ stepladder and 12,000 Lumen light fixture.  The light fixture is being powered from an extension cord plugged into the one duplex receptacle that was installed by the electrician as part of the service entrance. The bottom cords of the roof trusses are 16′ above the floor.

As I mentioned in the regular post for February 01 – 21, we picked up the 14’ Werner 2-sided step ladder from Lowe’s a few days ago.  I managed to get the new ladder opened and raised into position by myself, but going forward I plan to always have someone help me put it up, take it down, and move it around, unless I can find a wheel kit for it.  Otherwise, it’s really too much ladder for one person to handle safely.  I used it to hang a 120-Watt, 12,000 Lumen, 5000K integrated LED flat panel light fixture that I bought a few weeks ago at Rural King.  I had already attached the plug cord that came with it, and wanted to test the beam pattern and brightness when it was suspended just below ceiling height (about 15’6”).

 

 

 

WEDNESDAY 08

The dually tire tracks leading into the drainage ditch.

When the snow had melted, I discovered that one of the utility trucks had driven into the ditch along the road where the new pole was stored, and driven back out right over the end of the culvert under the driveway, partially crushing it.  Ugh.  I took photos and e-mailed a couple to the case manager who had been assigned to our project and asked what, if anything, DTE might be able to do about this.  Other than not ever getting advanced notification when crews would be here working, this was the only damage that had occurred to our property during the whole project.  And the culvert wasn’t crushed shut, so it could still drain, but this damage should not have occurred.

The dually tire tracks in the drainage ditch clearly headed up and over the end of the culvert into the gravel driveway.

Sometime after that, but still in the first two weeks of the month, I got another customer satisfaction survey from DTE.  This one acknowledged that the project to replace the pole/transformer and get power to the barn had been completed, and asked for feedback.  So, I provided it.  Well, once again, I got a call from a customer service representative.  In fact, it was they same women I had chatted with the first time.  My complaint by that point was that the case manager had not replied to my e-mail, even though the last communication I got from her said to contact her if there were any remaining issues.  She said she would escalate that and check on the other pole that was sitting in our yard.

The top center of this photo is the east end of the culvert under the driveway.  A little bit of the metal is visible, but the top was squashed down and it is mostly covered and filled with mud.

 

FRIDAY 10

The builder’s Pettibone Telehandler on site, waiting to help install the two large roll-up doors.

Although it took some doing, the builder (Chuck) managed to get his Pettibone Telehandler relocated from a jobsite in Washtenaw Country to our driveway in front of the barn.  This machine weighs about 28,000 pounds and has to be moved by a tractor on a flatbed equipment trailer.  Chuck has a guy he uses for this work, and today was they day they were able to get it arranged.  The telehandler will be needed to install the two larger roll-up doors, which are now in the possession of Everlast Doors & More, the local company through which they were ordered, and who will install them (with Chuck’s assistance).

 

Special Blog Post for 20230131 – Accessory Building Project Update

There are no photos for this post. ]

TUESDAY 31 January

Looking back on the last two (2) weeks, it had been an amusing, confusing, slightly sad, but exciting and gratifying time.  The electrical service work for the barn (with upgraded power for the house) was done.  The crews had all been very professional and had done the work well.  But they were also friendly and helpful, as they put up with my presence, questions, and photography with good humor.

The only question that remained, power wise, was when a crew would show up to change out the pole in the SE corner of our yard.  This pole does not have a transformer on it, but it does have the tap for our Comcast/Xfinity broadband cable to the house.  It supports the electric distribution wires that run E-W down our side of the street, along with the AT&T and Comcast cables.  These lines also T-off and go across the street to a pole in our neighbor’s yard to supply services to their house.  It does not have a transformer on it, but it looked to me like the T would make installing a new pole tricky.  I guess I will find out just how it’s done when someone shows up and does it, assuming I am at home when the work happens.  Never once have we been contacted in advance to let us know that a crew was scheduled to be onsite.

…..

Special Blog Post for 20230130 – Accessory Building Project Update

This post has 9 photos. ]

MONDAY 30 January

Expect the unexpected, right?  For me, that’s inline with the idea that “things happen beyond our control, but how we deal with them is up to us.”  After a week of somewhat strange communications, but no additional work, a crew from Rauhorn showed up today.  Rauhorn is another DTE contractor.  I think they do both overhead and underground work, and were prepared for both, but the remaining work was mostly underground.

The small excavator was used to “hang” the large spool of 3-conductor, 3/0 AWG service conductor cable so it could unwind easily as it was fed into the 2” Schedule 40 PVC electrical conduit through the bottom of the meter enclosure.  The conduit is visible coming out of the bottom of the meter enclosure and into the ground.

 

I was already familiar with Rauhorn as they did some of the work on the power upgrade for our neighbor’s house across the street back in mid-November.  When they were finished doing that work, I asked the crew chief if he had a few minutes to came over and look at what I was planning to do, conduit-wise.  He did, and gave me some very useful suggestions as to how to do it to make it easier on whatever underground crew eventually showed up to install the electrical cable to the barn.

The trench from the open end of the conduit towards the pedestal with the service conductors already pulled through.  The open end of the conduit is at least 24” below grade, but they did not trench that deep all the way to the base of the pedestal.  There is no conduit from this point to the pedestal, as the cables they installed are rated for direct burial.  That also means it does not matter if dirt or water gets into the conduit.  The conduit was optional, but it saved me the cost of having DTE (or a contractor) dig the whole trench, allowed me to route the cable away from some trees, and will provide external protect in the event that someone ever decides to dig in this area.

 

 

This crew was here “to complete the installation of power to the barn,” but were surprised to find that major pieces of the work they planned to do had already been completed, specifically the pedestal and the 350 kcmil service drop conductors.  (I was not surprised that they were surprised.)  But they were fine with the situation.

 

 

 

 

 

 

 

 

 

 

The trench for the barn service conductors to the base of the pedestal.  The top cover of the pedestal has been removed to allow access to the junction blocks.

 

 

I explained about the advice I got from one of their guys before trenching in the 2” Schedule 40 PVC electrical conduit, and pointed out the stake that marked the location of the free end near the new pole.  With the small excavator (12” bucket), they came prepared to dig a trench, but only had to use it to unearth that end of the conduit (and hang the large cable spool).  They dug up to the base of the pedestal by hand as there were live conductors buried there.

 

 

 

The 3-conductor, 3/0 AWG service conductor cable being fed into the 2” Schedule 40 PVC electrical conduit through the bottom of the meter enclosure.

They were glad to have the 7/16” rope already through the conduit and used it to pull the 3/0 AWG, 3-conductor underground service conductor (USG) cable from the meter enclosure up to the pedestal.  To does this, they suspended a large spool of the USC cable off of the excavator bucket so that it could unwind horizontally.  The free end of the cable was attached to the rope in the meter enclosure in such a way that it would not pull loose.  One guy helped guide/feed the cable into the conduit attached to the bottom of the meter can, while two guys pulled it through the conduit from the other end by hand with the rope.  They stopped with enough cable still at the meter enclosure to make the connections to the meter lugs.

 

 

The barn service conductors through the conduit and up through the pedestal.  They were then trimmed to the length needed to fit into the junction blocks.  At this point, the crew was dealing with live (energized) un-fused wires.  They knew what they were doing, and had the right personal protective equipment, but this was still not work for the faint of heart.

On the other end, they opened the top pedestal cover and routed the cable from the barn up through the bottom and out the top.  They cut each wire to length to fit into the large junction blocks that were already there.  As they were working, I noticed that one of the hot conductors that had been terminated by the previous crew had about an inch of exposed conductor below the insulated junction block.  That was a major oversight that could have led to a short or an energized pedestal cover (the covers are made of metal).  Rather than try to cut the live exposed metal strands shorter, one of the guys removed the conductor from the junction block, wrapped electrical tape around it up past where the wire insulation ended, reinserted it, and tightened it.  He was wearing proper personal protection equipment, (PPE), and clearly knew what he was doing, but all of this was on a live, unfused wire.

 

 

The barn service conductors enter the meter enclosure from the large conduit on the left and are attached to the meter socket lugs at the top.  (Meter enclosures/sockets have been built this way for a long time, going back to when almost all utility conductors ran overhead and entered the meter enclosure from the top.)  The black, red, and bare/aluminum conductors attached to the bottom meter lugs are the service entrance conductors.  They are enclosed in a sheath as they exit the meter enclosure at the lower right and go through a hole in the side of the barn, where they are then routed up into the bottom of the main load center and connected to the main breaker (first disconnecting means) at the top of the enclosure.  Because this is a sheathed cable assembly, it is not required to be in conduit.  Although I would have preferred that it was, this work was done by the electrician, under permit, and inspected/approved by the County.  As such, it was not appropriate for me to change it (and would have been a bit of work to do so).

 

 

ep was to install a meter, at which point we finally had power to the barn!  I closed the main circuit breaker (which serves as the main disconnect for the barn) and then closed the circuit breaker for the Siemens FirstSurge surge protection device.  Two green lights indicated that I had power to both buses of the panel.  (I later checked the GFCI receptacle the electrician had installed way back when, and confirmed that I had 120 VAC and the GFCI feature worked.)

 

 

 

 

 

 

 

 

 

 

 

 

 

 

The trench with the barn service conductors bending into the bottom of the pedestal. This photo shows that the wires, which are direct -burial, are not buried very deep at this point.

 

 

 

The final step was to put the upper cover back on the pedestal and secure it, and use the excavator to push dirt back into the trench and up to the base of the pedestal.  One of the crew members said they would transmit the meter number to DTE.

 

 

 

 

 

Almost done.  They meter was seated in the socket and, just like that, we had power to the barn!  It was obviously nice to finally have power to the barn, but the five (calendar) days it took to do this work were fascinating for me to watch and document.  I learned a lot from the various crews, who were all (mostly) good sports about me being around with a camera and asking lots of questions.

As the trench by the pedestal was being filled back in, I took this photo to show that the bottom cover of the pedestal does not extend very far below grade, and the wires going to barn bend almost immediately as they leave the pedestal towards the conduit.  The same is true for the service conductors going to the house.  Any digging within a 5’ radius of this pedestal would risk contact with these conductors.  They are all insulated, of course, but still …

 

I e-mailed the DTE case manger and the planning consultant (with a couple of photos) to let them know the work had been completed and I had power to the barn.  As far as I knew, I was now done dealing with DTE other than to get the account number for the new meter and pay the bill each month.

 

 

The meter enclosure cover installed and secured.

Although I was not going to pull an electrical permit until mid-March, and probably not start wiring the barn until early April, it was time to work on the electrical plan in earnest.  As soon as we returned from our travels I would need to be ready to start buying electrical materials and devices and staging them in the barn.  Of course, I needed the big roll-up doors in order to do that.

Special Blog Post for 202301(24-29) – Accessory Building Project Update

There are 3 photos in this post. ]

TUESDAY 24 January – SUNDAY 29 January

When the Motor City Electric Utilities crew finished their work on Monday the 23rd, the project was well on its way to completion, but not quite finished as we still did not have power to the barn.  During the week, I got an e-mail from our DTE planning consultant with contact information for the “case manager” who would schedule the work, and letting me know that I would now be dealing with her from now on.  I e-mailed her and introduced myself, and cc:d the planning consultant.  I included photos, and let them know the work was almost completed, and that all that remained to be down was to pull the underground service conductors from the barn meter enclosure to the pedestal, terminate them at both ends, and install the meter.  Once again, the reply that I received was basically “what?”

By this point, and after discussion with some friends, I had come to the conclusion that my customer satisfaction survey reply, and subsequent conversation with a customer service representative, appeared to have triggered a response from DTE.  While I was glad that the work was getting done, I was saddened that the people responsible for planning and scheduling the job, and with whom I had worked closely, appeared to be unaware that the work was taking place.  Indeed, the planning consultant indicated that he had only just released the work orders for scheduling.  And that was not right; it’s never right to bypass people.  Go through the reporting chain to the people responsible and make a higher priority of the work, sure, but do not go around them.

Sometime during this week, the builder also got word that the roll-up doors would not be available by the end of the month and he was trying to pin down a delivery date.  At this point, it almost didn’t matter.  We would be traveling from late February to early March, and I would not be starting the wiring until we got back.  In fact, I had to do some painting even before the electrical work, which I couldn’t do until the temperatures were warmer and would stay that way overnight.  Also, I had no interest in doing electrical work in the cold and neither did Marty, who offered to come down and help.

The main load center for the barn with the Siemens FirstSurge device mounted externally, lower right and connected to a 2-pole, 20 Amp circuit break, lower right in the enclosure.  This was the only wiring I intended to do on the barn before apply for an electrical permit in mid-June, but I wanted this device in place before the electrical service was energized.

I did, however, manage to accomplish two small things in the barn this week.  A while back I bought a Siemens FirstSurge Type 2 “whole house” surge protective device (SPD) and wanted to install it in the main service panel for the barn before utility power was connected to it.  Type SPDs get installed after (downstream of) the main disconnecting means, which in this case is the 200 Amp main breaker in the Siemens load center.

The unit is large at approximately 3” x 6” by 2” deep.  It is a sealed unit, with four wires coming out a female threaded stud.  I had intended to mount it directly to one of the knockouts on the load center, using a male threaded adapter from inside the enclosure, but I ultimately decided against that approach.

As shown in the photo, I ended up mounting it with four screws to one of the horizontal skags that the enclosure (and the siding) is attached to, and connecting it to the enclosure using a 12” piece of liquid-tight flexible non-metallic conduit.  The two hot leads from the device were wired to a 2-pole, 20 Amp circuit breaker, installed in the lowest two positions in the right circuit break bank.  (The neutral and equipment grounding conductors were terminated in the usual way.)

Type 2 SPDs are also available in circuit breaker form, which is the most convenient way to add one to an existing panel.  However, I really liked the more robust specifications of the FirstSurge device.

The sub-panel on the south wall of the shop just east of the door.  This is a lug-style panel (no main circuit breaker) that will be fed from a 100 Amp 2-pole circuit breaker in the main load center through fairly large feeder cables.  Although both the bus and the travel trailer have 240V/50A (120V/100A) electrical systems, most of the power used in the barn will be used in the shop.

 

 

The other thing I accomplished in the barn was hanging the sub-panel in the shop.  No wiring was involved; just deciding exactly where I wanted to place the enclosure.  I wanted it to be convenient to the door, but comfortable, as I will be using many of the circuit breakers as switches.  But I also had to make sure the location was compliant with the NEC.

 

 

 

 

 

 

 

Last, but not least, I continued to read the 2023 NEC Handbook and started working again on the electrical plan for the barn, as well as researching light fixtures and other devices for the project.

As an aside, The Motor Cities Electric Utilities crew on the 23rd, reattached the riser conduit for the AT&T cable and terminal box to the new pole as best they could.  They stapled the cable to the pole about a foot above the terminal box, as that was as much slack as they had to work with.  If you look closely you can see the wire goes directly (through air) from there to the junction block on the main cable.  It should be stapled all the way up the pole, but that will require a longer wire.  I was told that it would be up to AT&T to remedy this, ditto for Comcast if it involves their cables, but that I might have to call these companies myself and be “persistent” in getting them to come out and do something about it.  Ugh.  I just don’t see why I should have to deal with that situation.  Presumably DTE reports to Comcast & AT&T that they have replaced this pole and additional work needs to be done.

Special Blog Post for 20230123 – Accessory Building Project Update

There are 19 photos in this post. ]

MONDAY 23 January

Digging to find the underground service conductors and the AT&T cable from the house.  The wooden stake with the red tip, behind the crew member, is where our DTE planning consultant thought the ground pedestal should (might) be located.  The stake to the right, with the orange top, marks the location of the free end of the 2” Schedule 40 PVC electrical conduit that Marty and I installed back on November 22nd.  A comparison with the three (3) previous special blog posts makes in clear that we had snow yesterday.  Still, the crew said the ground was not frozen and was easy to dig.  They extended their digging from the old pole to the new one, as new wires would be run in that area.

I

 

did not expect work to be done on Sunday, and none was.  I also did not know when a crew would be out next to continue the project, but I did not have to wait long to find out.  Around 9:30 AM, a three-person crew showed up from Motor City Electric Utilities, a DTE contractor.  They arrived with a crane/auger truck and a bucket truck, but they also had a trailer with a small excavator (back-hoe) with a 12” bucket.

 

 

 

 

 

 

 

 

 

This photo is from the south facing north.  The new pole is on the left.  The existing underground service conductors from the house are clearly visible running up the old pole on the right.  The AT&T cable is also visible at the right/lower end of the small PVC conduit lying on the ground.

The insulated disconnect pole is hanging from the neutral distribution line after being used to disconnect power from the house.  The crew member in the bucket is dis-mounting the Comcast cable from the old pole, using the bucket to lift it up, and mounting it to the new pole.

 

The first thing then did was start hand digging (with a shovel, obviously) by the old pole, looking for the underground service conductors from the house.  The AT&T line to our house (no longer in service) also runs underground, along the same/parallel path as the power lines. (The service conductors for the house run underground from the meter, at the SW corner of the garage, to the old pole and then up to the transformer.  I presumed these were one continuous run, but splices were eventually found underground at the base of the old pole.)

 

 

 

 

The lower/AT&T cable being moved up and anchored to the new pole.

The next thing they did was open the disconnect switch so they could work safely around the conductors from the transformer secondary taps to the house.  But first they worked on disconnecting the AT&T and Comcast cables from the old utility pole, raising them up, and securing them to the new pole.  As part of this work, they had to route the existing AT&T cable down the new pole as best they could.  (The Comcast/Xfinity cable comes to our house from a different pole in the SE corner of our yard.)

 

 

This crew used the hoist on the end of their crane truck to support and lift the broadband and phone cables.  The latching hook is the orange thing visible near the center of the photo.

 

At this point, the existing house underground service conductors were disconnected from the new transformer and the old pole, and cut off about 4’ above where they exited the ground.  The AT&T cable was also disconnected from the old pole, but not cut.  (Note that our Comcast/Xfinity cable comes to our house from a different pole in the SE corner of our property.)  With everything disconnected from the old pole, the crane truck was then used to pull it out of the ground then lay it down.  It was then lifted and put on a pair of racks on the crane truck to be taken away.  The hole left by the old pole was partially filled in, but was reused to install the new ground pedestal (junction box).

 

 

The crane truck is used to pull the old pole out of the ground.

 

 

 

 

 

 

 

 

 

 

The bottom section of the old pole is loaded onto carrying racks on the crane truck.

 

 

The crew had decided early on that they were going to install the new ground pedestal (junction box) in the hole left by the old pole.  At this point, they dug up the underground service conductors from the house for a few feet back from the pedestal location.  A new cable assembly, consisting of three (3) 350 kcmil conductors, was then routed down the new pole to provide the service drop to the pedestal.  (At 350 thousand circular mils, these are big multi-strand conductors.)

 

 

The 3-conductor, 350 kcmil cable that will run from the rack to the pedestal.

 

At the upper end, the three wires were joined to the secondary transformer wires at the rack.  The bottom end was left loose initially.  The support post for the pedestal was then set into the ground and the conductors from the pole and the house positioned so the bottom pedestal cover could be attached.  The two sets of wires were then spliced together using very large, insulated terminal blocks for the hots and an uninsulated junction block for the neutrals.  The upper cover was put in place and secured, and all areas that were still excavated were filled back in.

 

 

 

Two of the crew set the support post for the pedestal, part of which is lying on the ground to the right.  The large 3-conductor 350 kcmil cable has not been cut to its final length, positioned underground, and secured to the new pole.

 

 

 

 

 

 

 

 

 

 

 

 

The underground service conductors from the house have been routed up into the bottom have of the pedestal and the crew is working to free the AT&T cable so they can move it out of the way and relocate it to the new pole.

 

 

 

 

 

 

 

 

 

 

 

 

This X-shaped cable stripper was the biggest wire stripper I have ever seen.  The house service conductors were 3/0 AWG, smaller than the 350 kcmil conductors the ran down the new pole, but still big.  (The 350 kcmil conductors will supply power to both the house and the barn.)

 

 

 

 

 

 

 

 

 

 

 

 

The junction blocks used to connect the cables together are visible in the center of the photo.  The orange thing is the handle of a large T-style hex wrench.  The junction blocks for the hot conductors are insulated, the one for the neutral is not.

 

 

 

 

 

 

 

 

 

 

 

 

A closer view of the junction blocks in the pedestal as the upper cover is put in place.

 

 

 

 

 

 

 

 

 

 

The 350 kcmil conductors are positioned underground and the first piece of protective PVC cover is secured to the pole.

 

 

 

 

 

 

 

 

 

 

 

A final look at the large conductors (for now) before they are re-buried.

 

 

 

 

 

 

 

 

Filling in the hole and making it safe.

 

 

 

 

 

 

 

 

Using the bucket, the protective covering for the 350 kcmil cables was attached all the way to near the bottom of the rack.  The conductors were then spliced together with the conductors from the transformer secondary taps at the rack.

 

 

 

Last, but not least, the disconnect switch was closed and utility power was restored to the house.  I e-mailed our planning consultant and included photos of the ending status of the work.

 

 

 

 

 

 

The finished installation connecting the new transformer/rack on the new pole to the new pedestal and the existing house underground service conductors.  The disconnect switch has been closed, and the house is back on utility power.

Although the crew was done working on the DTE-related project of getting power to our barn, they were not done working at our property.  The repositioned their equipment near the SE corner of our property and proceeded to grab one of the new 45’ utility poles from the ditch down the street and drag up to our place.  They had a work order for this pole as well, and used their crane truck to pick it up and deposit it in our yard.  They then spent a bit of time looking at the pole they had to replace.    In the end, they left without doing anything else, but I don’t know why.  Perhaps they did not have everything they needed, or it was just too late in the day to start.  It looked like a tricky job to me, as power, phone and broadband lines T off at this pole and go across the street to the pole that supplies our neighbor’s house.

 

 

Done for the day, and moving on to the next thing.

As always, I e-mailed our DTE planning consultant and included a few photos of the work.

Special Blog Post for 20230121 – Accessory Building Project Update

This post has 11 photos. ]

SATURDAY 21 January

Friday came and went with no additional work being done, and no indication of when another crew would be on site, but sometime in the morning, a different DTE crew showed up, again with multiple trucks of various kinds.  Working from a bucket truck, they opened the disconnect switch, disconnecting power from our house.  The whole-house generator quickly came online and took over providing power to the house.

Bucket trucks positioned for the aerial work.  The bucket on the left has an insulated pole that was used to operate the disconnect switches (old and new).

Their first task was to disconnect the conductors from the existing transformer primary to the two distribution lines.  The bucket was then used to support each line (in turn) as it was disconnected from the existing insulated stand-off and then lifted up and attached to new insulated standoff on the new/higher crossbar.  This increased the height of the lines over our center driveway and over the road to the west where it cuts through the SW corner of our property.  Indeed, getting these lines raised was one of the reasons the existing pole was being replaced.  The other reason was its age and condition.

 

The second bucket getting ready to go up.

 

 

 

 

 

 

 

 

 

 

 

 

 

 

Two buckets, each securing on one of the distribution lines to the new cross-bar.  The line on the left is the “hot” (notice the disconnect switch).  The line on the right is the neutral.  Besides being connected to one of the primary taps on the transformer, the neutral is bonded to the bare copper ground wire that was installed the full length of the new pole and establishes a local earth reference for the voltage.

 

 

 

 

 

 

 

 

 

 

 

Disconnecting the old transformer.

One of the bucket trucks was positioned to disconnect the house underground service conductors from the existing transformer secondary taps and then dis-mount the existing transformer while the other one, which included a hoist, was used to support and lower the old transformer as it was removed from the old pole.

 

 

 

 

 

The old transformer on the ground.

The old pole was then “topped” a few feet above the AT&T and Comcast cables.  The new 50 KVA transformer was then hoisted up and hung on the new pole.  The rack was already installed just below it, but I’m not sure when that happened.  The rack is a large vertical assembly with three (3) insulated standoffs.

 

 

 

 

 

 

The new transformer being hoisted into position.  Note that the new transformer is pre-wired with both primary and secondary conductors.  Note also that the old pole has been “topped” to make more room for the buckets to get into position.

 

 

 

 

 

 

 

 

 

 

 

 

Both buckets work together to get the new transformer on the previously installed mounting bolts.

The primary taps of the transformer were connected to the neutral conductor and the disconnect switch for the distribution lines and the wires from the secondary taps were secured to the rack.  The ground conductor was also attached to the distribution neutral and the secondary center-tap on the transformer.  The existing service conductors for the house were then temporarily routed to the rack and connected to the secondary transformer conductors.  The disconnect switch was closed, and power was restored to our house.

 

 

 

 

The bucket that was used to hoist the new transformer up was also in the best position to attach the wires from the secondary taps to the insulated stand-offs of the rack.  The rack has three stand-offs, one for the neutral conductor and one for each of the two hot (240 V) legs.

 

 

 

 

 

 

 

 

 

 

 

 

In this photo, the existing house underground service conductors (USC) have been temporarily spliced to the new transformer secondary conductors at the rack.

 

 

 

 

 

 

 

 

 

 

 

In this photo it is a bit clearer that the house underground service conductors are still attached to the old pole.  The Comcast/broadband (upper) and AT&T (lower) cables are also still attached to the old pole.

 

 

 

 

 

 

 

 

 

 

 

 

The crew is done for the day and pulling out.  Our house is now running off of the new 50 KVA transformer.  I checked inside and the voltage seemed to be a volt or so higher, and less subject to dropping when loads were energized.  (We have uninterruptable power supplies throughout the house to protect sensitive electronics.  The units we use have a digital voltage display, so I can keep a close eye on what’s happening vis-à-vis electrical power.  We also have a DTE EnergyBridge device, which monitors and reports our electrical energy usage in real time, via our smart meter, but also gives us access to historical data.)

Significant progress was made today towards having upgraded power to the house and, eventually, to the barn.  I e-mailed the planning consultant and included a couple of photos.

Special Blog Post for 20230119 – Accessory Building Project Update

There are 6 photos in this post. ]

THURSDAY 19 January

The DTE crew that was here yesterday and did, in fact, return today and got a lot accomplished.  Not everything, of course, but based on what had previously been explained to me, I did not expect them to complete the job today.  DTE has crews (and/or contractors) that do “overhead work,” crews/contractors that do “underground work,” and (apparently) crews/contractors that do “fusing work.”  Which is fine; each of those kinds of work requires different equipment, knowledge, and skills.  Our project required all three types of crews (or at least overhead and underground ones).

The new, 45’, utility pole in the driveway near the existing pole and the new hole that was dug yesterday.

The new pole is lowered onto a cradle, allowing the top (narrower) end to be off the ground high enough to attach various things to it.

The work today was fascinating.  They started by pulling the new pole out of the drainage ditch (where it had been for a while), down the street, and then up the driveway.  They positioned it in the yard close to where they needed it, but off of the driveway where they could work on it without being in the way of the trucks.  Crew members drilled holes for the mounting of the new crossbar, transformer, and the rack and attached a bare copper ground wire along the full length of the pole.

The new pole resting on the cradle.  The cradle is hinged, and folds flat for storage.

One of the crew attaches an insulated stand-off to the crossarm near the top of the new pole.  The insulated standoff and disconnect switch for the hot line are already installed.

A new crossbar was attached near the top of the pole and new insulated standoffs and a disconnect switch for the distribution lines were mounted.  The crane truck was used to hoist the pole up with the crossbar parallel to the distribution lines so it would pass between them.  The pole was then lowered down into the new hole (dug yesterday) and then turned 90 degrees so the crossbar was above, and perpendicular to, the power lines.  They sighted the pole for plumb from two directions, about 90 degrees apart.  When they were satisfied that it was vertical, a 2-part epoxy was mixed and poured into the hole.  After a suitable amount of time, they then partially back-filled the hole with 1”-size gravel to secure it in position.

 

 

 

The crane truck has lifted the new pole between the distribution wires with the crossarm parallel to the wires and going up between them.  Ground crew have then turned the pole 90 degrees so the crossarm is perpendicular to the wires.  The crane has set the pole into the new hole.  The crew member nearest the camera is checking the pole for plumb.

The new pole was 45’ long, compared to the old one at just 40’.  They were both in the ground to about the same depth, and the top of the new pole was now a comfortable 5’ above the top of the old one.  This added height was one of the main reasons for the new pole.  The other reason was the condition of the existing pole, which had been there since the early 1970’s (best estimate).

 

All of this work was done without disconnect the existing transformer primary taps from the distribution lines.  The crew obviously knew what they were doing, and had all of the necessary personal protective equipment (clothing) to be working with energized, un-fused, high-voltage wires, but it was still impressive to watch.

 

The new pole, secured in the new hole, with the primary taps on the existing transformer reconnected to the distribution wires.  The service conductors for the house are still attached to the old pole, as is the AT&T cable.

With new pole secured in the new hole, the disconnect switch was closed, restoring utility power to our house.  The power was only disconnected for about an hour, but the house was never without power as the whole house generator started up and ran flawlessly the whole time.

 

Again, I e-mailed our planning consultant to let him know what had been accomplished today and included a couple of photos.  Again, he seemed surprised.  I thought that was odd, but I was just pleased that crews were at our house and the work was getting done.

 

 

Special Blog Post for 20230118 – Accessory Building Project Update

[ There are 6 photos in this post. ]

WEDNESAY 18 January

Without any notification, a 4-person DTE crew showed up around 9 AM with three huge trucks and a pick-up truck.  I presumed they were here to start replacing the existing utility pole and transformer that feeds our house with a new, taller, pole and a new, (much larger), transformer, as this  new transformer will now also supply power to the new barn.  I bundled up and went out to introduce myself.  I would hang with them for the duration of their visit, chatting with them about the work and taking photos.

The vacuum excavator (hydrovac) truck arrives.

The hydrovac truck in position by the existing utility pole.  Some of the DTE trucks are also visible.

One of the trucks was a crane with an auger, but they did not use it.  They had to dig a hole for the new pole close to the existing pole, which meant it would also be close to the existing underground service conductors from the house.  In this situation, they prefer to dig the hole with a “hydrovac” (water jet / vacuum) truck.  Even though the location of the underground wires had been marked by MISS DIG, the DTE crew said the marker flags can be off by several feet from the actual cable location.  Ditto for the underground AT&T cable.  DTE uses a contractor for the hydrovac work, and a truck was on the way from Roseville on far east side of the Detroit Metro Area.  (We are on the far west side of the Detroit Metro Area).

Operating the hydrovac truck is a 2-person job; one of them controls the high-pressure sprayer and vacuum tube, while the other one controls the equipment at the truck.

The first 12” of the vacuum tube (orangish color) is a hard metal collar with a fairly keen edge, allowing it to “cut” into the ground while retaining its circular shape as the dirt is loosened by the high-pressure water spray.

The hydrovac truck eventually arrived, got positioned to do the work, and proceeded to dig a 6.5-foot-deep hole some 12” – 16” in diameter, about 30 inches to the west of the existing pole.  As the dirt was blasted loose, the vacuum hose sucked it up, along with anything/everything that came loose, including some larger rocks.

It took at least 90 minutes to dig this hole, which surprised me, but the operators worked carefully to get it right.  There wasn’t much for the DTE crew to do while they waited for this hole to be dug.  One of the bucket trucks, however, had the new 50 KVA transformer, and that crew member went ahead and prepared/attached the small conductors that would go from the primary taps to the distribution wires and the large conductors that would go from the secondary taps to the “rack” below the transformer on the new pole.

[ As an aside, we have two main load centers in our house, a 200 Amp panel in the basement and a 100 Amp panel in the garage.  Although we would never draw the maximum combined amperage of 300 Amps, even at an 80% derated current of 240 Amps these panels represent the possibility of a 57,600 VA (Watt) load on the transformer.  The barn has a 200 Amp main load center, which at an 80% derated current of 160 Amps, represents the possibility of another 38,400 VA of load.  Combined with the house, that would be a possible 96 KVA load.   The existing transformer is a 10 KVA unit, and is being replaced with a 50KVA unit.  This will be a good size, in my opinion, but not overkill. ]

(The distribution voltage is 13,200 Volts (13.2 KV), but the current through the primary coil of the transformer is relatively low, so the wires do not have to be very large.  If the transformer was operating at its maximum rating of 50,000 Volt-Amps (50 KVA), the current in the primary wires would be about 3.8 Amps.  By comparison, the voltage between the two “hot” secondary taps is 240 Volts.  If the secondary was supplying the full rated capacity of 50 KVA, the current in the secondary conductors would be about 208 Amps.  That amount of current requires really big wires.)

Conductors attached to the secondary taps of the new transformer.

In what was the first of several “comical” events (from our point of view), the crew was scheduled to be at a required training session in Pontiac at noon, at least a 30 to 40-minute drive from our house.  They left sometime after noon and headed there.  Things got done, but far less than if they had been able to stay and work.  As they prepared to leave, they said they would be back the next day.

 

 

 

 

 

The hole for the new utility pole covered and marked for safety.

I was pleased and excited that the work had finally begun.  I e-mailed our planning consultant, as he had indicated early on that I should let him know as things happened and send a few photos.  The reply I got was, essentially “what?”

 

 

 

Special Blog Post for 202301(06-17) – Accessory Building Project Update

[ There are no photos with this post. ]

As described in a regular blog post, we left for the long drive to Florida on Monday, December 26, picking up our middle grand-daughter on the way.  We stopped for the night in Chattanooga, Tennessee and arrived at our destination in Orlando the evening of the 27th.  We started the return drive home on Tuesday, January 3 (2023) and spent that evening in Macon, Georgia, with a stop the next evening in Covington, Kentucky just across the river from Cincinnati, Ohio.  We arrived home the afternoon of the 5th, after first returning our grand-daughter to her parental units and younger sister.  The barn project was not on our minds (much) during this time, as we were visiting “the happiest place on earth” with our 10-year grand-daughter while hanging out with our friends, and Eastern/Atlantic travel companions, Nancy and Paul, and their family.  No progress was made on the barn project during this time, nor was any expected.  We knew before we left that the roll-up doors had been delayed until (at least) the end of the month.

FRIDAY 6 January – TUESDAY 17 January

This was mostly a waiting period, but I did stay in touch with our DTE planning consultant.  No pressure, though; winter had settled in and I would not be doing any electrical work on the barn until spring.  Also, my copy of the 2023 NEC Handbook had arrived just before Christmas, so I spent a lot of time reading this 1339-page book.

The NEC is incredibly comprehensive, covering residential, commercial, and industrial electrical installation.  I paid particular attention to the residential requirements, of course, but read much of the other material as a matter of curiosity.  In spite of two degrees in Electrical Engineering, my exposure to power engineering is limited, and I am certainly not an electrician (which is a primary audience for the NEC).  As I would be doing the final wiring of the barn, I was glad to have the time to study the CODE.  The Handbook version is longer than the basic CODE book, and especially nice as it contains a lot of additional commentary, drawings, and photos, to clarify and illustrate much of the CODE text.

During this window, we received a generic customer satisfaction survey from DTE.  We have been pleased with the quality of power we receive, the response to outages when they have occurred, and the attention to preventative maintenance, such as tree trimming, so I filled out the survey to reflect our general satisfaction with the company.  There was a box at the end asking if there was anything other feedback we wanted to provide.  Well … since you asked.  While my interactions with our DTE planning consultant have been positive, and I said so, I was disappointed that the company was “quick to take our money, but slow to do the work, and that I had no idea when the work would actually be done.”  I clicked “SUBMIT,” figuring nothing would come of it.

Well … I got an e-mail acknowledging receipt of the survey and thanking me for taking the time to submit it.  An automated response, I presumed, so again, I did not expect anything to come of it.  I then got an e-mail indicating that my comments had been reviewed and that someone would be contacting me.  “OK, sure” I thought.  But someone did call.  We had a nice chat, which I appreciated as I had a chance to explain more clearly the feedback I was trying to provide.  Again, I figured that would be the end of it.  Not long after, however, the project took a decided turn, and I will cover that in the next five (5) special blog posts on this project.

Special Blog Post for 202212(01-31) – Accessory Building Project Update

[ There are 3 photos for this post. ]

As November gave way to December, it became clear that we had reached the stage in this project where sayings such as “the last 10% of a project takes 50% of the time” always seem to come into play.  Not labor hours, of course, but calendar time, and visible milestones, for sure.  The building is constructed; the electrical service entrance (meter enclosure, main panel, and outlet/receptacle) is installed, inspected, and approved; and the driveway is finished (for now).  Separate from the building contract, the 2” Schedule 40 PVC electrical conduit has been trenched in from the meter enclosure to near the existing utility pole.  Other than wiring the building, which is on me to do, it looks/feels like we are very near completion of the builder’s portion of the project, but big things remain to be done.

FRIDAY 02 December

Chuck, the builder, let me know that he had finally gotten an estimated availability date from the vendor for the two large roll-up doors … December 28th (of this year).  There is always a list of a few minor things that need to be done or corrected, but these doors are one of the two remaining major components of the actual building construction, the other being the gutters.  At this point, I presumed that they would not be installed until early in the New Year.  Work on this project started in the second half of June, not long after we left for our 4-month journey through Eastern/Atlantic Canada, so mid-January would mark the seven (7) months point.

TUESDAY 06 December

Today was a big day; we finally received the costs to have the electric power on our property upgraded and extended to the new accessory building (RV barn, workshop, storeroom).  Also, sometime today (or yesterday) the gutter sub-contractor was apparently here and installed the gutters and downspouts on the two long sides of the barn.

WEDNESDAY 07 December

Today was, perhaps, an even bigger day than yesterday, as I finally received the actual contract for the electric utility work.  All that remained to do was read it carefully, sign it, scan the pages, and e-mail them back to a special e-mail address at DTE Energy.  I looked the contract over, especially the costs.  The language used throughout the documents was specialized for DTE’s purposes, but I had a sense of what was what, and everything appeared to be in order.  I was missing a diagram that the cover letter said I was supposed to have, and had a few other procedural questions, so I e-mailed our DTE planning consultant back.

The most expeditious way to move things along was to scan the signed documents and e-mail them back.  This would trigger a reply e-mail with a link to a special payment website.  I decided to hold off submitting everything until tomorrow so I could read all of the boilerplate contract language.

The way the project was now moving, and with real winter just around the corner, it appeared that I might not get any wiring done in the barn until spring.  Since I would have time between now and then, I had been considering purchasing the 2023 version of the NFPA 70 / NEC (National Electric Code) Handbook, which will be available on December 15, 2022.  It’s a bit spendy, but the Handbook contains the complete text of the CODE along with extensive inline commentary, diagrams, and photos that “explain/illustrate” what the CODE language means, and how it is applied in practice.  That sounded like some interesting and meaningful “home study” over the early winter months.

The builder was here today to see what was wrong with the shop and storeroom doors, and fix them if possible.  Before looking at the doors, we were both surprised to see that the gutters had been installed (on the long sides of the building).

Both doors are very difficult to open, and both of them have dead-bolts that will not slip into their strike plates, even with jiggy-jogging them.  Chuck determined that the difficulty in opening was due to bottom sweeps that were a bit too thick, although they might become a bit more compliant with use and age.  The sweeps snap in and out fairly easily, and he will try to get slightly thinner replacements for both of them.

The storeroom door appeared to be installed correctly, with an even reveal between the door and the frame on the inside and with everything square.  The solution for the dead-bolt will be to grind the strike plate, which is OK with me.  (It’s what I would have done if I was fixing it.)  He would have to come back to do that.

The Shop door, however, was not installed correctly, being slightly out of square and not having an even reveal between the door and the frame from the inside.  Chuck said he would be out in the next few days to remove it and reinstall it, or have one of his carpenters do it.  It’s already trimmed out, so I don’t know if that means removing and reinstalling all of the trim, but he said it was the only correct way to fix the problem.

THURSDAY 08 December

Linda had to go into the bakery today, so during the first part of the morning I read over the entire DTE contract package.  I then signed it in the two places that I needed to, and scanned those two sheets, saving them as PDFs and renaming them for clarity of content.  One was the “Line Extension Agreement” and the other was the “Secondary Services Agreement.”  I attached both PDFs to an e-mail and provided additional contact information per the information from my DTE planning consultant, and sent the e-mail off to the special DTE e-mail address.  I wasn’t sure how long it would take for DTE to respond, so I left to run some errands.

While I was out, I got a text message with the payment link.  So far, so good.  When I got home, I also had an e-mail with the payment amount.  But I had a second e-mail indicating that I had not submitted all of the required documentation.  I spent the second half of the afternoon scanning the rest of the pages into PDFs, renaming them, attaching them to an e-mail (along with some additional information), and sending it off to the special DTE e-mail address.  By then, it was late enough in the day that I was tired of dealing with this and ready to sit on the sofa and work a puzzle or watch a Youtube video while I waited for Linda to get home.

After an easy dinner of salad and pizza, Linda used the payment link and paid the invoice.  Correct documents or not, they were more than happy to accept our money (CC).

I will check e-mail tomorrow morning to see if I got it right on the 2nd try.

FRIDAY 09 December – WEDNESDAY 14 December

Well, the contract was accepted as complete and we received verification that our payment had been received.  I contacted our DTE planning consultant to let him know.  He replied back that it might take a couple of days for him to receive official/internal confirmation, at which point he would generate the work orders needed for the project.  That internal communication eventually took place, at which point I was notified that the work would “probably” be completed by the end of January, but not later than 17 February (2023).  That was discouraging to hear, but this was the first time I had dealt with DTE on a project like this, so I was not familiar with all of the steps or the timelines involved.  Regardless, it was out of my control.

The free end of the conduit near the utility pole with the 7/16″ rope passed through the hole in the end cap and everything taped to prevent dirt and water intrusion.

Sometime prior to the 14th, the DTE planning consultant made another site visit to have a second look at the utility pole replacement and the conduit we had installed from the pole to the barn.  Because the conduit runs downhill from the pole location to the meter location, he suggested I try to seal up the open end by the conduit as best I could to prevent water/dirt from getting in.  Given the time of year, if water got into the conduit and froze it would prevent the cables from being pulled through and we would have to wait until the spring thaw to get the service conductors installed from the pole to the barn.  He also marked the location for the ground pedestal (junction box), but indicated that the crew(s) that did the work might place it in a slightly different location.

 

 

A view of part of the trench, filled in and raked out.

Marty and I had placed a 7/16” rope in the conduit after we assembled it and put it in the trench.  One end was tied around the lugs in the meter can, and the other end came out the open end of the conduit and up a wooden stake marking the end of the conduit, as we planned to bury it, where it was tied at the top so the end could be easily located later.  I had tried to seal the open end with a rag, but this was not adequate.  I had a cap with a domed end, so I drilled a 1/2” hole in the end of it, fed the rope through the hole, and slid the cap over the end of the conduit.  Although not glued, it was a snug fit.  I taped around the rope at the hole, and around the cap and conduit with Gorilla tape.  I retired the rope to the wooden stake, and then buried everything.

The trench beyond the free end of the conduit has been back filled and marked with a stake that secures the rope. Plywood has been put down and covered with plastic and dirt to keep as much water out as possible.

 

 

 

 

 

 

 

 

 

THURSDAY 15 December – SATURDAY 31 December

With the holidays coming, and a trip planned between Christmas and early January, not much else happened on this project the rest of the month.  The builder was notified that the roll-up doors were now delayed until the end of January, 2023.  Oh well.  Again; out of our (and his) control.

Special Blog Post for 202211(15-30) – Accessory Building Project Update

[ Note:  This post mainly consists of 26 photos with captions.  All of them were taken on a Google Pixel 6 Pro smartphone and processed using Faststone Image Viewer. ]

 

TUESDAY 15 November – WEDNESDAY 30 November

As previously noted, the electrical service entrance was prepared on Thursday, November 10.  By this time, the weather was changing, becoming cold enough that I could no longer paint.  Any painting that remained to be done, such as the outside of the two interior shop/storeroom walls, and the sides of the staircase, would have to wait until spring 2023.  With my painting activities curtailed for the winter, and with the electrical service entrance work done, I turned my time and attention to designing the electrical plan for the building using QCAD.  Indeed, I started with the building floor plan, turned off details that were not relevant, and added new layers for all of the electrical stuff.  Outlets, switches, a sub-panel for the shop/storeroom, and wiring would be fairly straight forward; it was just a matter of how many devices, where they would be placed, and how/where the wires would be run.  Lighting, on the other hand, lead me down something of a rabbit hole researching lighting requirements and fixtures.

With a 16’ clearance to the bottom of the roof trusses, I need to use “high bay” light fixtures for the RV bays.  These fixtures are much brighter (8,000 to 35,000 lumens) than the typical “shop/utility” tube lights used in many residential garages and workshops (2,000 to 4,500 lumens).  Selecting fixtures that will work the way I need them to, required me to jump back into lighting parameters such as illumination (in lumens), color temperature (in degrees Kelvin), Color Rendition Index (CRI), beam patterns and coverage (as a function of height above the working surface), mounting/wiring methods, suitability for use in unconditioned spaces (the RV bays), and energy efficiency.  The last one was easy, as all of the lighting that I install will be LED, which has a 10:1 energy advantage over tungsten filament bulbs.  (LEDs use ~1/10 the energy of a tungsten light source for the same amount of illumination, or provide 10x the amount of illumination for a given energy consumption.)  LEDs also have a lifespan that is 10 to 50 times that of tungsten bulbs, and come in a variety of color temperatures, specifically 5,000 K (Daylight) which is appropriate for areas where work is being done.  A comparison to fluorescent lighting would probably be more appropriate, but LEDs still come our way ahead on all of these parameters.  I will have more to say on this subject once I have actually selected light sources.

 

The electrical service work (meter box, load center, and one duplex outlet) was inspected and approved on Wednesday, November 16.  This was a critical milestone in the project, as DTE Energy won’t do anything relative to getting power to the building unless/until this work is completed, inspected, and approved.  I e-mailed the DTE planning consultant (John B.) late in the evening to let him know this work was done.  Following this approval, I purchased the 2” Schedule 40 PVC electrical conduit and couplers from City Electric Supply in Waterford, Michigan.  They did not have the sweeps I needed, or the 22.5-degree elbows.  I found the sweeps at Lowe’s and/or Home Depot, but had to order the 22.5-degree elbows online (Amazon).

 

MONDAY 21 November

In spite of the cold weather, and 4” – 5” of snow on the ground, there was work that had to be done.  On the couple of occasions when it had snowed prior to today, I used a gasoline powered backpack leaf-blower to remove the snow from the electrical cable paths from the existing utility pole to the house (which had been marked by MISS DIG 811) and the area from the pole to the barn where I intended to dig a trench and install the conduit for the electric service entrance cable.

I had a few errands to run today, and when I returned I found two DTE subcontractor trucks parked in the street in front of our house, with one of them blocking the first driveway entrance.  That wasn’t a problem, as the bus is currently parked in front of the house and I had no immediate use for the first entrance.  Still, I was curious why they were there so I walked over and talked to the guy in the lead truck.

They had spent the morning working at our neighbor’s house across the street.  Our neighbors are the third owners of the first house built in this subdivision.  Built in the late 1960’s, the house still had its original 240/120V, 100A electrical service.  They are upgrading it to 200A, and that meant a new main panel, a new meter/box, a new transformer, and new cable from the pole to meter.  Their existing service was overhead wires from the pole to the house, but DTE will not upgrade those wires.  As with new construction (like our barn), they will only run cable underground from the pole/transformer to the meter on the side of building.  They also install a terminal strip on the pole a few feet below the transformer and connect the wires from the house and the transformer together at the terminal strip.  These particular sub-contractors where an “underground” crew and had spent the morning digging a trench from the pole to the meter location, installing direct-burial cable, leaving enough of it coiled up on a hangar on the pole to reach the terminal strip, and then back-filling the trench.  A DTE crew will come out and remove the old overhead cable and transformer, mount the new transformer and terminal strip, route the new cable up the pole, and make all of the connections.

The sub-contractors were on a break, and I asked if the guy would be willing to take a few minutes to look at my situation.  The thing that has been a source of confusion for me was where to end the trench/conduit, and what direction it should be pointed.  My DTE planning consultant had simply indicated “about 10’ from the existing pole.” But that lacked the specificity that I wanted as we were (apparently) also getting a new/taller utility pole that would (probably) be installed “about 5’ to either side of the existing pole.”  It would, of course, be in line with the existing overhead cables (power, broadband, and phone).  I knew that DTE would also install a ground mounted junction box/pedestal and that the wires from the house, barn, and transformer would be joined in this box.  But it was not clear exactly where the pedestal would be placed relative to the existing pole, much less the new pole in an as yet undetermined location.  My confusion/concern was also partly fueled by not having ever dealt with this before and not understanding exactly what was actually going to happen.

The sub-contractor looked at my proposed path and filled in a few critical pieces of missing information.  I learned that the junction box would (likely) be installed about 3’ from the new pole, directly away from the edge of the driveway.  If I located the end of the conduit in-line with a line offset from the existing pole by 3’, and stopped a few feet short of the possible closer junction box location, it would be a perfect setup for a crew (like his) to do what they need to do.  I also learned that they will NOT install additional conduit from my conduit to the junction box; all the cable they use is rated for “direct-burial” and does not actually require conduit.  (Conduit is nice, however, especially in rocky soil or other situations where it might be subject to damage.)  They will simply trench from the end of my conduit to the junction box/pedestal location, as well as from the pedestal location to the new pole location.  Finally, he assured me that I would not have any difficult bending the 2” Schedule 40 conduit along my indicated path.  Based on what I learned, I staked out the actual path for the trench/conduit from the barn to near the existing utility pole, using landscape flags.

 

TUESDAY 22 November

Today was spent digging a trench and installing approximately 90 feet of 2” Schedule 40 PVC electrical conduit, including a 36” radius sweep (quarter circle) and a 12” long 22.5 deg elbow.  The conduit will house the service entrance cables that the power company will run from the pole to the building.

My friend and fellow converted bus owner, Marty, who is a licensed electrician, agreed to come over and help with this task.  I was glad to have the help.  The work proved to be quite physical, and often required coordinated effort; I doubt that I could have accomplished it by myself.  Linda also helped, off and on throughout the day, taking breaks from her accounting work to take photos, fetch things that we needed from the garage, fixing a light lunch, and taking on the task of cleaning the rented trencher with our power washer once we were done digging.  (We had chosen this day to do the work because the high temperature was going to be well up in to the 40’s.)

But before that happened, I used yellow marker paint (spray can designed to work when inverted) and “painted” the path that I had marked with flags yesterday.  I then unloaded the 36” trencher from the trailer as I wanted to be ready to work as soon as Marty arrived around 9 AM.

 

On Monday evening, November 21, I rented a 36” trencher from the local Home Depot for 24 hours.  This would allow us to use the machine all day and still be able to clean it and return it on time.  (The 24-hour rental was only 22% more than the 4-hour rental.)  This particular machine digs a trench approximately 5-1/2” wide.  This photo is from 8:30 in the morning as I prepare to back the trencher off of the tilt-bed trailer, which was part of the rental.  The machine was chained down to the trailer for transport.  The only issue I had was releasing the tension on the front chain, but I eventually figured out how to loosen it.  (Photo by Linda.)

 

I had never operated a piece of equipment like this, but last night I studied the directions that came with it, and it seemed straight forward enough.  In this photo, I have backed the trencher up enough to cause the trailer bed to tilt down and touch the ground so I could back the trencher off onto the driveway.  (Photo by Linda.)

 

Marty and I decided to dig the trench for the conduit starting at the meter and working towards the utility pole.  In this photo, I am driving the trencher over to the meter box location.  Although not obvious from these photos, the overnight low temperature was in the low 20s (F) and the ground was initial quite firm.  It was not deeply frozen, however, and was easily dug.  By late morning the temperature had risen above freezing and we had a clear sky with a bright sun.  All of the areas of bare dirt (not grass) within a 15-foot radius of the meter box turned to mud, which only got worse as the day went on, with a high temperature in the low 40s (F).   (Photo by Linda.)

 

When digging, the trencher is driven backwards.  The operator stands on the platform at the rear and can see the digging chain when it is raised, but cannot see it when it is lowered.  I’ve just dug a short section of trench coming out from the riser conduit into the meter box, and have lifted the chain out of the ground.  Where the chain meets the body of the trencher (yellow) a horizontal auger is just visible.  When digging, the auger moves all of the dirt off to the left (when facing forward).  Visible on the safety bar above the blade is a piece of white tape.  It was already there when I picked up the machine, but turned out to correspond to an ~27’ trench depth, which is what we were aiming for.  DTE Energy requires the top of the conduit to be at least 24” below grade.  (Photo by Linda.)

 

I did not get a photo of the control panel, but it consisted of a choke and throttle for the engine, a control lever to lower/raise the blade, two drive controls for the left and right drive treads (like a bulldozer), and a lever to engage/disengage the chain.  The engagement lever moved sideways, and had to be pulled over with my right hand and held there while also operating the right drive tread.  It was actually easier than it sounds, and I got the hang of operating this beast fairly quickly.

 

Marty spots me to get the tip of the blade as close as possible to the riser conduit into the meter box, and let me know when the blade was at the correct depth.  (When the blade was lowered and digging, I could not see any of it, including the piece of white tape that served as our depth gauge.)  Because the trencher is driven backwards while digging, I was able to see the yellow stripe (about 2” wide) through the operator platform, which was perforated and ridged for good traction.  (Photo by Linda.)

 

Conduit assembly started at the meter box end.  I held a 36” radius sweep against the riser conduit into the meter box with the other end at the bottom of the trench while Marty marked the point where we needed to cut the riser so we could join it to the sweep.  The upper portion of the riser had a threaded fitting already installed into the meter box.  A nut inside the meter box threaded onto the fitting to secure the riser to the box.  (We set the lower portion of the riser aside after cutting it, and eventually used it as the last piece of conduit at the pole end.)  In this photo, we are adding a 22.5 deg elbow to the end of the sweep.  I held one end of the sweep against the side of the barn so that it was parallel (vertical) while the other end rested on the concrete apron (horizontal) and Marty loosely fit them together and marked them at the position where the elbow was flat on the concrete and bending in the correct direction.  We then lay the pieces down on the apron for assembly.  We could not trench in a direct line from the meter box to the pole because of several trees, but the combination of the sweep and the elbow got the conduit pointed in the direction of the straight portion of the trench.  Part of the trench is visible behind Marty.

 

This is a view of the trench from near the existing utility pole.  (This pole will be replaced with a taller one located within 5 feet either side of the existing one.)  The end of the conduit is propped up above the trench so we can add an additional piece to it.  The first 30’ (approx.) after the sweep/elbow is straight and angled away from the trees.  It then curves around the trees in a broad sweep.  At the pole end, the conduit is running approximately parallel to the edge of the driveway and about 3 feet farther away than the pole.

 

DTE requires a minimum depth of 24” from grade to the top of the conduit.  This photo shows that we are at 27” (the trench depth varied from 27” to 30”).  A single piece of this 2” Schedule 40 PVC conduit does not appear to be at all bendable.  However, the DTE contractor that was here yesterday assured me that a longer run would bend just fine for the curve I had marked out.  We added two 10’ pieces (“sticks”) at a time, and then pulled it around into the trench with no difficulty, keeping the free end out of the trench and resting it on a shovel handle set across the ditch so we could install the next piece(s).

 

This is the utility pole end of the trench/conduit.  The stake marks the end of the conduit.  We used a 125’ steel “fish tape” to pull a 100 foot, 7/16” rope through the conduit from the pole end and into the meter box.  (This rope has a 300 lb. pull strength.)  Marty handled the meter box end while I fed the rope into the conduit.  There was approximately 4 feet of rope at the meter box, which Marty wrapped around the meter socket before putting the cover back on.  I had about 6 feet of rope at the pole end, which is just visible in the lower right corner of the photo.  The white object in the trench is a cotton rag that I stuffed into the end of the conduit to keep dirt out.  The end of the conduit is about 6 feet from the existing utility pole (5’ to the west and 3’ to the north.  Everything after this will be done by DTE or their sub-contractors.

 

WEDNESDAY 23 November to MONDAY 28 November

I was sick with an upper respiratory viral infection during this time (and beyond), and nothing else much was accomplished on the barn.  I did learn on Monday that the ETA for the two large roll-up doors is now December 28 (of this year).  I also emailed our DTE planning consultant to let him know the conduit was installed in the trench and included pictures, as requested.  He indicated that he would (finally) do our plan/quote on Monday, November 28.   On Monday, I also heard from Phil at Precision Grading that he would have the 21aa stone delivered tomorrow and be on site to finish the west pull-through driveway extension to the barn.

 

TUESDAY 29 November

Phil arrived around 10 AM.  He got his front-loader and bulldozer unloaded from his equipment trailer and then unloaded a large roll of road/construction fabric from the box of his dump truck using forks on the front-loader.  I made myself available to help with placing the road/construction fabric, but otherwise spent most of the day cleaning up the dirt along both sides of the conduit trench.  This included gathering up medium-to-large rocks and using them as fill for the somewhat larger hole near the meter and along the first 5’ of the trench.  I took occasional breaks to take photos of the driveway work.  We both finished up around 4:30 PM.  It was a long, hard day, but a lot got accomplished.

 

This is a view looking SW from the SE corner of the bar showing the first pieces of road fabric in place on the “1×3” stone and crushed concrete base layer.  Phil is standing in front of the front loader at the left of the photo.  His dump truck and equipment trailer are in the street.  The bulldozer is barely visible at the far corner of the barn.

 

This is a view looking W from near the existing utility pole at the edge of the existing west pull-through driveway.  The area covered by the road fabric is the new driveway extension/approach for the barn.  This is where most of the new gravel will be placed.  This new area will slope down to the SW, away from the barn and from the yard to the right in this photo.  (Note that the yard to the right will drain to the NW and surface water will flow N along the east side of the barn and then flow W past the rear of the barn.  Phil had previously graded the area around the barn, but will return at some point to add soil and regrade this area to ensure proper drainage.)

 

This is a view looking NE from the SW corner of the existing pull-through driveway.  The curved edge of the new area to the left is to accommodate the left steer tire of the bus when swinging around from the pull-through driveway to pull into the left RV bay.

 

This is a view looking SE from the SW corner of the barn.  The pull-through driveway slopes down from just before the existing utility pole all the way to the street.  The yard on the other side of the new driveway extension slopes towards the camera and to the left.  The new driveway extension slopes away from the barn and away from the yard to the right and down towards the street.

 

This is a view looking SW as the gravel train prepares to back into the driveway and dump the gravel from the rear trailer.  Phil will help the driver get it positioned so that the gravel pile is mostly on the road fabric.

 

The first load of stone has been dumped and the truck is pulling out while lowering the trailer box.  The driver pulled to the far side of the street and then unhooked the rear trailer so he could back in and dump the main truck box.

 

This is the second load of stone and is being dumped from the actual dump truck.  The two piles of gravel visible here contain a lot more gravel that it might appear (approximately 20 cubic yards, or about 60,000 pounds).

 

In this photo, Phil is using the front loader to scoop up the gravel and move it to various locations on the road fabric.

 

Here, Phil is using the front-loader to deposit/spread the 21aa stone.

 

Phil needed more stone to finish the job.  He had some at his shop, which isn’t too far from our property, so he dropped his equipment trailer and took his dump truck to get it.  His stone is darker than what was delivered earlier, due to being a bit wet.

 

Once all of the gravel was placed and spread somewhat evenly, Phil switched to the bulldozer to grade it.

 

Besides getting a relatively flat surface and consistent thickness, Phil used the bulldozer to carefully grade the stone along the edges.  The bulldozer is very heavy, so it also created some compaction of the stone.

 

Buy the end of the day, the new driveway extension was a surface that could be driven on comfortably, but was not as compacted as I wanted it to be.  In the next few days, I would use the F-150 to drive back and worth over the gravel from a variety of directions to pack the surface, but that’s for a future post.

 

WEDNESDAY 30 November

One of the carpenters from Patriot Builders was here today to install the locking door knobs and deadbolts for the entry, shop, and storeroom doors.  The three door knobs and two deadbolts (shop and storeroom) were all keyed alike.

 

Exterior view of the shop door with the locking door knob and deadbolt installed.

 

Exterior view of the storeroom door with the locking door knob and deadbolt installed.

 

Interior side of the entry door with the locking door knob installed.  Besides the window, this door has deeper jams to match the thickness of the wall, protruding 1/2” into the interior to accommodate drywall or plywood, should we wish to add that in the future.

 

The exterior side of the entry door with the locking door knob installed.  This slightly broader view shows the panel detailing on the lower portion of the door and a bit more of the window.

Special Blog Post for 202211(01-14) – Accessory Building Project Update

[ Note:  This post consists of 13 photographs with captions.  All photos were taken on a Google Pixel 6 Pro smartphone and post-processed with Faststone Image Viewer. ]

 

TUESDAY 01 – MONDAY 14 November

 

A view of the shop looking toward the NE corner from the door in the SW corner.  The ceiling/joists and walls have been primed with Killz-2 using an airless sprayer and then painted with Valspar Pro Storm Coat Exterior semi-gloss acrylic white paint.  The spray nozzle clogged frequently and the whole process was messy and inefficient.  Still, it was probably better than doing the joists and the OSB on the ceiling with a brush and roller.

The stairs to the storeroom.  The risers have been primed and painted white.  The treads have been primed and painted light gray using Valspar Pro Deck, Floor, & Porch anti-skid paint.  The stair walls and the spaces at either end of each step have been trimmed in 1x pine but have not yet been primed/painted.  The doors for the shop and storeroom have been installed.

The extension of the west pull-through driveway to the front of the barn.  Phil (Precision-Grading) was here most of the day on the 5th, initially redistributing the 1×3 crushed concrete based, and then finish grading the dirt on the other three sides of the barn.

The view of the accessory building from the NW after the finish grading.  The grades on the E, N, and S sides were sloped away from the building a bit more and tapered gradually into the existing terrain.  That created some extra dirt in addition to the large and small piles that were already there.  Phil had me designate low areas to fill in, and I selected ones that were both obviously in need of some fill and not too far from the building to make it efficient for him.

The main/permanent entry door for the barn.  The carpenters removed the temporary one and replaced it with this one.  Besides the class window, this door has extra deep jams which will allow it to be properly finished off if I ever decide to install paneling/drywall and trim.

Looking straight up the stairs to the storeroom, the risers and trim have been primed/painted white and the treads have been primed/painted light gray with anti-slip floor paint.  Although not visible, the landing at the top of the stairs and the floor of the storeroom have also been primed and painted with the light gray anti-slip paint.  Everything will have two coats of paint when the job is done, although some of that might not happen until spring 2023.

The carpenters trimmed between the OSB and the stairs, under the trim on the top and front of the walls, and along the floor.  I was able to get all of this primed and painted (one coat) before the weather turned too cold.  The Valspar Pro Storm Coat paint can be applied down to 35 degrees (F), but the weekend after these photos were taken, the lows started dropping into the mid-to-low 20s (F) at night and only rising into the 30s during the day.  That signaled the end of the painting until spring.  As is obvious in these photos, the larger walls that enclose the shop and storeroom have not been primed and painted yet, a big job that will have to wait until next year.

The electrician (Bill) was finally able to fit our barn into his extensive commitments and install the service entrance.  Seen here is the meter can and riser conduit on the SE corner of the building.

The meter can with the cover removed.  The black and red wires are the two ‘hot’ leads (L1 and L2) and the bare aluminum wire is the neutral, all going to the load center on the other side of the wall.  The conduit lower/left is where the wires from DTE will come into the meter can and attach to the lugs at the top of the box.  The meter blades will plug into the four vertical spring-slots and then the cover will go back on and be secured by DTE.

The electricians had to chisel out part of the foundation to allow the riser conduit descend vertically (more or less) below ground level.  I will install the 2” Schedule 40 PVC Conduit that connects to this pipe and runs through the yard to junction box by the utility pole (once it is installed).  I will rent a trencher from The Home Depot in Howell for this work.  The horizontal white device is just a clamp for the ground wire.  The wire coming up from this device goes through the wall and into the bottom of the load center; it does not go through the meter can.  It leaves the clamp through the bottom and then runs to the right where it attaches to two, 8’ long copper ground rods driven into the ground next to the foundation.

The top few inches of both ground rods are visible, as is the bare copper ground wire that connects them to the ground bus (and case) of the load center.

Shown here is the Siemen’s 240/120V – 200A Load Center.  The service entrance cable and ground wire come through the wall and up into the bottom of the load center.  Just visible at the top/right is a yellow 12-2+G Romex cable that feeds a duplex outlet out of sight to the left of the photo.

I put in a request for the Miss Dig 811 service late last week with a work start date of November 10.  I had to create an account and do the whole thing online, but it was otherwise a fairly smooth process.  The only caveat was that I could not draw the work area polygon using the pencil on my iPad Pro and ended up having to do the whole thing on my laptop computer.  The confirmation said the site would be marked not later than 12:57 PM on November 10.  The utility location service showed up around noon on that date, and was done before one o’clock.  The flags and paint for the DTE electric (magenta) and the AT&T phone (orange) cables to the house are marked.  (The AT&T cable is no longer in use.)  We have natural gas and broadband cable on the property as well, but they are on the other end of the house, well away from the work area, and did not need to be marked.

 

Blog Post for 202210(18-31) – Accessory Building Project Update

[ Note:  This post covers updates on the accessory building (barn) project for the 14 days from Tuesday, October 18 through Monday, October 31, 2022.  There are three photos with captions. ]

 

TUESDAY 18 October

The accessory building (barn) is so close to being done that I am getting a bit impatient for it to actually be finished.  Which is to say, to have all of the stuff the builder is taking care taken care of.  Once he is done, there will still be a lot for us to do, but most of it cannot be started until all the permitted details are complete and he has gotten the final inspections.  Top of the list, for me, is all of the electrical work that I still have to do, and the first step is arranging for our electric utility, DTE Energy, to run power to the building.  I put in my service request with them on Wednesday, October 12, and expected to hear back from a planning consultant not later than tomorrow.  I now have to design the electrical plan, which I will do in QCAD (the same software I used to design the building).

In the meantime, the one thing I can do is prime and paint the walls in the shop and storeroom, as well as the risers on the stairs, and then prime and paint the floor in the storeroom and the treads on the stairs.

 

WEDNESDAY 19 October

The HVAC technician (Mike) from Lakeside Services (Lakeside Heating and Cooling) arrived around 1 PM today to service the Bosch hot-water baseboard heating system for the house, and the heating portion of the Bryant HVAC unit for the library.  He was here until about 3:30 PM.

I spent most of the day at my desk working on the final post for our trip and a parallel post for the activities this past week related to the accessory building (barn) project.  I knew that the electrician might be here sometime this week, and by mid-afternoon I had it in the back of my mind that I should   check to see if he was on site.  I went outside around 2:45 PM and saw several vehicles down by the barn, so I walked down to check it out.  I could hear the unmistakable sound of a circular saw, so figured it was probably not the electrician.  I was right.

What I found instead were three vehicles and three carpenters.  The crew chief was Rob, who is Patriot Builders lead finish carpenter.  (Chuck, the owner, is a framing carpenter, and Garrett, who I met last week, does both framing and finish work.)  A bit to my surprise, they were installing OSB on the inside of the studs for the sides of the staircase, and also installing OSB on the interior of the shop and storeroom walls.  I had not realized they were going to finish off the stairs, and had (apparently) forgotten that they were going to finish off the walls.  All of which was great.  I had a brief, but very nice, chat with Rob and then left them to work in peace without any more interference from me.  I texted Chuck to let him know the guys were here and that I met them briefly.

 

THURSDAY 20 October

Sometime around this date the DTE planning consultant assigned to our work order showed up on site (unannounced).  I was in the middle of painting, but obviously stopped to give him whatever time he needed.  We had a very nice chat about what I was trying to accomplish.  By the time he left, it was clear that he wanted to have DTE run power to the barn from the same transformer that powers the house.  It also appeared that he had determined that we needed a larger transformer, but also needed a new utility pole, possibly taller than the current one, located within ~5 feet of the current one.  As best he could tell from the ground, he thought our current transformer was 10KVA and said something about switching it to a 25KVA.  He indicated that wire from the junction box to the barn would be $10/foot (I would need close to 100 feet) and there would be a charge for the new/larger transformer, but probably not more than $1,500.

I pointed out that the house already has a 240V/200A main load center and 240V/100A, secondary load center (not a subpanel), and that the barn would have a 240V/200A load center as well.  I noted that 24KVA is only 100A at 240V (or 200A at 120V), so a 25KVA transformer would still be far below the capacity of my three load centers, and that my total existing loads exceed the load center capacities.  This is actually typical, as load centers never draw their full rating, and probably rarely draw half of their full rating for more than a short period of time.  Still, as long as we are going to the trouble and expense of doing this work, I wanted to make sure the new transformer was adequately sized.  (My research later revealed that the next size up from DTE is 50KVA.)

As I understood the order of events, it would go something like this:  0) Get confirmation that the meter can, load center, and an outlet have been installed in the barn by a licensed electrician and the installation has been inspected and approved by the permitting authority (Livingston County Building Department, in this case).  1)  Deliver new pole to the site.  2) Install the new pole, transformer, and terminal strip.  3) Install a junction box in the ground about 5 feet from the new pole.  4)  Disable the power to the existing transformer.  5)  Move the existing wires to the new pole.  6) Run wires from the new transformer to the terminal strip.  6) Run new/large wires down the pole from the terminal strip to the junction box.  7) Connect the existing wires from the house to the junction box.  8)  Pull the new wires for the barn from the meter box to the junction box.  (I will have the 2” PVC conduit already installed in a trench.)  9)  Install the new meter for the barn.  10)  Energize the new transformer.

He indicated that it would likely be a month before this got done, but to get the process moving along, and provide me with the cost estimate, he needed the LOAD SHEET, asap.  He also ‘suggested’ that I include any/every thing I thought I ‘might’ possible ever want to power.  I got the sense that this LOAD SHEET was part of a justification/approval process for the cost of whatever work has to be done, determining what our share of that initial cost will be, and what payback the utility company can expect.

I already had the LOAD SHEET pdf, and it indicated that most of it has to be filled out and signed by a licensed electrician.  I explained that the meter can and load center were being handled by the builder’s electrician, but that I did not have my own electrician for the job.  I explained that I have an EE background, but am not an electrician, and asked it would suffice for me to fill it out myself?  He didn’t say ‘no,’ which I took to mean ‘yes,’ or at least ‘okay, not great, but I’ll work with that.’  He also made it clear he needed it sooner rather than later.

From this meeting forward, I continued painting during the day when it was warm enough and I had some daylight to work with.  In the evenings, I worked on determining the loads I would need to power and filling in the LOAD SHEET.

 

FRIDAY 21 October

The floor joists for the storeroom floor are exposed on the underside in the shop, and I do not plan to install a flat ceiling onto them.  With that in mind, I thought it might be easier to prime/paint the joists and the underside of the OSB storeroom floor with a paint sprayer.  I don’t own one and have never used one.  Thinking this might be a one-time use, not wanting to spend a fortune, and not having an air-compressor with adequate CFM or an oil/water separator/filter, I got a Wagner Control Pro 130 airless sprayer at the local Lowe’s.  I chose Killz-2 for the latex primer and Valspar Pro Storm Coat semi-gloss acrylic latex for the paint.  Even though I will be using the paint inside, this exterior paint is formulated to deal with outdoor temperatures with cracking.  It can also be applied down to 35 degrees (F), so well suited to what I needed to accomplish given the time of year.

 

FRIDAY 28 October

Towards the end of the afternoon, I finally uploaded the LOAD SHEET to my DTE planning consultant, along with an Excel Spreadsheet I had created to catalog my current and future loads, both for the house and for the barn.

 

MONDAY 31 October

For the balance of this post, I am going to just include a few photos.

The south/interior wall of the shop with a view through the door to the area under the storeroom stairs.  Closed-cell spray-foam insulation is visible between the floor joists for the storeroom above.  The walls have been spray-foamed and then covered with OSB.

The stairs leading up to the storeroom as seen from the large/west bay door opening.  The side paneling and studs have been removed under the high end of the stairs.  The area under the landing has never enclosed as the door the to shop is there.

The storeroom looking SW from the NE corner.  The floor has been masked off at the base of the walls for painting.  Likewise, the Velox sun-tunnel diffuser in the center of the ceiling has been masked off.  The transparent painter’s plastic had the unexpected benefit of spreading the light out more towards the walls.  The step ladder is a 6-foot model.  The ceiling height is ~7 feet.

 

Blog Post for 202210(18-31) – Back to Normal (for now)

[ Note:  There are no photos for this post. ]

 

TUESDAY 18 October

Life is gradually returning to normal, which is to say, we are moving back into the rhythm of our normal, daily routines, local activities, and commitments.  Not completely, of course.  Adapting back to home life after an extended trip takes time, and we are not necessarily in a hurry to complete the transition.

Linda placed an order last night with one of our local Panera’s for a baker’s dozen bagels, to be picked up this morning, so she fetched those first thing.

A technician from Schutz Heating & Cooling was supposed to be here this morning between 8  and 10 AM.  Sometime between 8 and 8:30 I got a phone call from the company.  The technician had called in sick and they needed to reschedule.  No problem, the appointment was routine maintenance, and was easily rescheduled for Tuesday, October 25 at 10 AM.

Around lunch time we drove over to the Oceola Township Hall and picked up our absentee ballots for the November 8 general election.  It turned out that our new voter ID cards had been returned to the Township as they were mailed while we were away but could not be forwarded to our daughter’s house.  The reason they could not be forwarded, and that we could not pick them up in person, was that they constitute a confirmation of address.  We confirmed that our mail was, once again, being delivered to our house, and the clerk said she would re-post them.

As part of the transition, bridging our travel adventures with our home routines, we met our friend, and my former co-worker, Kate, for an evening out at the Corner Brewery (Arbor Brewing Company) in Ypsilanti, Michigan.  Kate and Brian live in Ypsi, and she still works at Wayne RESA, so we typically drive in her direction about once a month and get together for food and beverages (usually beer) someplace relatively convenient for her.

We left around 4:45 PM in a light drizzle and drove through mist and rain of varying intensity all the way.  We got to the pub around 5:30 PM and Kate joined us a little before 6 PM.  We always try to arrive early enough to get a booth (we didn’t) and get our first glasses of beer at happy hour prices (we did).  Linda selected a table near the booths.  A booth opened up before Kate arrived, so we snagged it.

It’s always a wonderful evening when we get together with Kate, and this was no exception.  She is an intrepid traveler, and has been following our trip blog with genuine interest (which I very much appreciate).  And we are always interested in where she has been recently, or plans to go next, as well as the goings on of her (very talented) nieces and nephews.  She had birthday presents for Linda, a couple of books, wrapped in paper that she had designed and printed herself (she’s a graphic artist) with a repeated pattern of an F-150 pulling an Airstream trailer.  Linda removed the paper carefully, treating it like a treasured object.  We had a couple of gifts for her as well from our travels.

We finally returned to our vehicles around 10:15 and headed home.

 

WEDNESDAY 19 October

The HVAC technician (Mike) from Lakeside Services (Lakeside Heating and Cooling) arrived around 1 PM today to service the Bosch hot-water baseboard heating system for the house, and the heating portion of the Bryant HVAC unit for the library.  When he tried to flush out any debris from the hot-water tank, he discovered that the floor drain in the furnace room appeared to be almost fully clogged.  That’s not a good thing, as the furnace is a high efficiency natural gas fired condensing unit, and the condensate drain line discharges into this floor drain.  The water from the floor drains (this one and the one in the laundry room) flow to the sump in the NE corner of the basement.  I could hear water dripping into the sump, but removed the lid to get visual confirmation as well.  We waited a while and the water level in the floor drain slowly dropped.  Obviously the rate at which the furnace puts condensate into this floor drain is slower that the rate at which it flows out to the sump, but not by much, and certainly not by enough.

Lakeside Service doesn’t not deal with drains, but Mike gave me the name and phone number of a company that does (Clog Busters).  He was here until about 3:30 PM.  The library furnace filter was fairly clean (last changed on May 24, 2022), but Mike suggested I get a MERV 11 filter element instead of a MERV 13, which he felt was too restrictive, and reminded me to replace the batteries in all of the thermostats.  We also talked about CO detectors, making sure we had ones that were sensitive enough to actually matter, and that we had them installed in the right places.  I will call the company Mike recommended to deal with the slow drain.  I could run a long hose out the downstairs doorwall to drain/flush the hot-water tank, but I will probably wait for the drain to be opened up.

I got a text message from Lakeside Service not long after Mike left asking me to provide feedback.  It was a positive experience, and I responded accordingly.

 

THURSDAY 20 October

We got our seasonal Flu shots and bi-variant CoVID-19 boosters at a local CVS this morning.

Sometime during the day, a Boondockers Welcome guest arrived.  It was someone we have hosted before, and we were glad to have her return.

I called Clog Busters, the company I was referred to by Lakeside Service, and set up an appointment for Monday morning.

In the afternoon, Linda met with Dave, the Controller from Metropolitan Baking Co., to pick up work and discuss a major upcoming software project.

Yup, we were returning to our normal routines.  Except for the barn, of course; having a building that size constructed on our property is not a routine occurrence, and there is nothing about the experience that is routine.

 

FRIDAY 21 October

According to our calendar, Linda met up with Diane to go for a walk today.  I am writing this post weeks later, and have no idea what else we did today.

 

SATURDAY 22 October

The two youngest grand-daughters arrived today for a sleepover.  Paul and Nancy also came over for dinner as they were in the area staying with their son and daughter-in-law in Ann Arbor.

The weather was also warm enough to paint, and looked like it would stay that way for the next few weeks, so I started acquiring the materials I would need to prime and paint the inside of the shop and storeroom, as well as the stairs, in the barn.  More on all of that in a separate barn update post.

 

SUNDAY 23 October

The morning after the sleepover night, Paul and Nancy returned to have breakfast and visit.  They enjoy interacting with our grand-daughters.  They eventually returned to Ann Arbor in the early afternoon.  We then gathered up the munchkins, drove them back to their house in Ann Arbor, and stayed with them for a bit before returning home.  On the drive back, the system information screen in the center of the dashboard (navigation, entertainment, information) went completely dark.

 

MONDAY 24 October

Today was a slightly less routine day.  First up was dropping off the F-150 at Brighton Ford for a service appointment.  The appointment was originally to do a LOF, check the brakes, make sure the SYNC 3 and navigation MAPS were up-to-date, and investigate the slight hesitation when going from 3rd to 4th gear while driving slowly with the powertrain not yet warmed up.  Since the info screen had apparently died last night on the way home, I added that to the list.  The drop off was a bit less smooth than usual, however.  When I made the appointment I was told to check in with a specific service advisor, the same person I have worked with exclusively for two years.  I arrived on time, and asked for that person.  He was busy, but that was fine, I wasn’t in any hurry.  When he finally got to me, he didn’t think he was my service advisor, and that I was supposed to work with someone else that I had never worked with before.  He agreed to do the write-up, however, but seemed pressed for time.  Whatever, I described the issues, signed the paperwork, and rejoined Linda, who was waiting for me in her car.  I should have read carefully what he actually wrote down, but I didn’t.

Clog Busters was scheduled to arrive as early as 10 AM, which they did.  The technician started by adding water to the floor drain in the furnace room, and confirmed that it was mostly clogged and draining very slowly.  He could see a lot of loose material at the bottom of the drain/trap, so he started by removing it, picking out the larger pieces and vacuuming out the rest.  He then ran a drain snake through the drain, and was able to feel a T-intersection, which I presumed was the drain running from the laundry room to the sump in the NE corner of the basement.  The snake opened things up a bit, but not that much.  He then ran the snake through the floor drain in laundry room, thinking it would emerge in the sump.  (It was my job to watch for it coming into the sump.)  At one point he had 100’ of snake in the drain tiles, but was never able to get it to emerge into the sump, even though I thought I could hear it.  In any event, by the time he was done the drains were emptying and flowing into the sump much better than they had been; probably for a long time.

We had in-home health assessments scheduled for 1:15 PM, and Clog Busters was done and gone before that.  The health assessments were a no-added-cost benefit of our health insurance plan/provider.  Having them done in-home was one of the options, so we gave that a try.  They were conducted by a P.A. and took about an hour for the two of us combined.  It was a very easy process.

Tuesday is garbage pick-up day, and the company (Granger) that bought out our service provider (Alchin’s) does our street in the first half of the morning.  That means the container gets wheeled to the edge of the street on Monday at 5 PM, so as not to forget it in the morning.

 

TUESDAY 25 October

Schutz Heating and Cooling arrived around 10 AM, as scheduled, to service the Mitsubishi-Trane heat pump they installed in October 2021.  Everything was OK with the unit in heating mode.  They will return in the spring to check/service it in cooling mode.

Nothing else of special note occurred today.

 

WEDNESDAY 26 October

We were notified by Xfinity (via e-mail, IIRC) that they were increasing our broadband speed, apparently at no extra cost to us.  Of course, our 1st year special pricing ended in July 2022, so we are now paying more for the service.  The notification said I had to restart the gateway to activate the higher speeds, so I did.  That’s always a bit of work, as I like to shut down all of the devices in the house, including the network switches, and then restart them in order:  gateway first, then the switches, then all of the devices.  The notification wasn’t completely clear if the speed boost would be immediate, or perhaps take place by “sometime in November.”  I ran a speed test anyway, and did not see any change from what we normally have.  I will try again in mid-late November.

I had not heard anything about the service work on the F-150, so I called the dealership later in the afternoon and spoke to my service advisor.  He didn’t have a current status, but said he would check on it and call me in the morning.  He did indicate that the reason he thought another service advisor was going to handle it was because of the transmission issue.  OK.  I wasn’t necessarily in a hurry to get the truck back, but it was unusual for them to have it for this long for relatively routine service.

 

THURSDAY 27 October

Linda has been doing a lot of work for the bakery and I have been working on whatever I can do in the barn.  I called the Ford dealership back to see what the status was on the F-150, only to find that my service advisor had not made it into work today due to a “family emergency.”  OK.  That happens.  I was directed to service manager, so I called him and left a message.  What unfolded from there was a text message conversation rather than return phone calls, which I thought was rather odd.  What I was told was that they had not been able to duplicate the “hard, delayed shifting from 3rd to 4th gear.”  I communicated back that this was not the problem I had reported.  Apparently, however, it’s what the service advisor had written down.  So, they had apparently spent time trying to replicate and chase down the wrong thing.

 

FRIDAY 28 October

Linda spent the day in Ann Arbor babysitting.  She took Halloween treats for the girls as we would not see them again until after that.  I worked on the painting projects in the barn.

At some point I was notified that the F-150 was done and ready for pickup.  Linda was home in time to drive me to the dealership.  All I had to pay for was the LOF service.  We bought the truck from this dealership, and have had all of the service done here except for the LOF and tire rotation in St. John’s Newfoundland back in August.  My interactions with the staff have always been pleasant, and the work has always been performed correctly and in a timely manner, the events of this week notwithstanding.

 

SATURDAY 29 October

We got together with neighbors this evening.  Marta was back temporarily from her contract assignment in San Francisco, so Gail arranged for a 6:30 PM get-together at their house with the usual suspects (Gail/Mike, Marta/Gary, Rose/Jerry, and us).  Mike already had a really nice campfire going when we arrived, and kept it well-tended all evening.  Everyone brought snacks to share and came bundled up against the impending cold.  It was great to re-connect, and catch up, with our neighborhood friends.

 

SUNDAY 30 October

Just another day in paradise, apparently.

 

MONDAY 31 October

Boo!  We have never had trick-or-treaters since moving to our current house, but to avoid any misunderstanding, we made sure the outside lights, and all of the lights on the main floor, were off and that the shades were closed.  We then retired to basement and watched TV.

20220825 – Barn Project Update

THURSDAY 25 August – Special Blog Post

As I mentioned in my regular blog post for this date, I checked my phone before going to bed and had a text message from our builder with four photos of the barn.  The windows were in and the siding was almost done.  It looked good, and should be a nice addition to our property and lives.  Here are the photos with a little additional information in the captions.

 

This is the view looking north at south/front elevation of the building, which faces the street.  The two large openings are for the 12’ wide by 14’ high RV bay roll-up doors.  The small opening in-between them is the entry door.  I tried to adjust the image so some of the interior detail might be visible.  The back, right corner of the building has interior walls from the floor to the bottom of the roof trusses, which are 16’ above the concrete floor.  The ground floor will be a shop, and the floor above it will be a storeroom.  The door into the shop is mostly in line with entry door and the door to storeroom is directly above it.  A staircase will go up the center of the barn to storeroom.  (Photo by Chuck-the-builder.)

 

This is the view looking SE at the NW corner of the building.  The narrow vertical features are fixed pane windows.  The three on the west (right) side and the one on the back will provide light to the full-depth (~46’) RV bay on the west half of the building.  The bottoms of these windows are 6’ above finished grade.  The small opening, lower left, is one of two double-hung windows for the shop.  (Photo by Chuck-the-builder.)

 

This is the view looking SW at the NE corner of the building.  Again, the narrow vertical features are fixed pane windows.  The two on the east (left) side will provide light to the (~30’) RV bay on the east half of the building.  The bottoms of these windows are also 6’ above finished grade.  Both of the double-hung shop windows are visible.  (Photo by Chuck-the-builder.)

 

Just for completeness, this is the view looking south at the north/rear elevation.  The windows are as previously described.  (Photo by Chuck-the-builder.)

20220803 – Barn Project Update

Special Blog Post for

WEDNESDAY 03 August

Here are some additional photos of the barn project from yesterday and today.  The first photo was taken by Keith, our lawn care guy.  The others were taken by Chuck, the builder.  The project appears to be moving along nicely.  While I would have loved to be on site to watch all of this happen, we are very confident that we chose the right builder for this project.

The trusses are up and the roof decking plywood is being moved up using a SkyTrack. (Photo by KK.)

 

 

 

 

 

 

 

 

The trusses from underneath, with the roof sheathing in place.  I love the framing stage of a building.  The plywood stops short of the ridge beam for the continuous ridge vent that will be installed.  (Photo by CS.)

 

 

 

 

 

 

 

 

There is a lot to see in this photo.  Two large RV doors with entry door between them on the south face.  Window framing on the right/east wall.  The general site and driveway preparation.  I put a lot of advanced design work into figuring out the location of the barn and the sweeps on the driveway extension to be able to get the bus and the trailer in/out of the barn easily.  (Photo by CS.)

 

 

 

 

 

 

 

 

 

 

The vertical metal siding will attach to the horizontal stringers.  The framing for the rear window is visible.  (Photo by CS.)

 

 

 

 

 

 

 

 

The SkyTrack on the west side of the barn.  The framing for the three windows on this side are visible.  (Photo by CS.)

 

 

 

 

 

 

 

 

 

2015/11/25 (W) T Minus 2 Days

We both got up at 7:45 AM.  My back felt OK when I went to sleep last night but it was not good by morning.  I don’t know if that is a result of being immobile and supine or just the Ibuprofen wearing off.  As painful as it is to get up it feels better once I do.  We both got dressed to work.  Linda prepared raisin toast and tea for breakfast while I positioned myself on the heater pad.  Linda was busy by a little after 9 AM and I was up and about by 9:30.

The first thing Linda did was take out the trash.  She called yesterday and stopped our pickups starting next week.  It took me an hour to finish organizing tools and supplies in the garage.  At that point I turned off the garage furnace and opened the overhead doors.  I started my car and turned it around with the back end facing the garage.  We moved all of the things that were going in the bus outside the larger door.  We then loaded a lot of the stuff into the car.  This is not a permanent arrangement but was merely for the convenience of getting packed for traveling.

I helped get the recycling tubs into Linda’s car.  Late morning she took them to the recycling center and stopped at two different banks to make club deposits.  I took care of some computer-based tasks while she was gone.  I finally got a reply from DataViz regarding a sync problem with Passwords Plus and sent the tech support person (Colin) a copy of the sync log from my computer.  I also managed to register the Sony flash and accessories I bought a month ago.  When Linda got back she made grilled cheese sandwiches for lunch and served them with fresh apple slices.  The cheese was Tomato Cayenne from Field Roast and it made for a tasty sandwich on rye bread from Metropolitan Baking Company.  I had a couple of Ibuprofen for dessert.

We disassembled the temporary work table in the garage and stored the sawhorses out of the way.  We shook out the floor mats (as best we could) and Linda used the ShopVac to vacuum the floor of the larger bay.  We finally had enough room to store her Honda Civic inside for the winter.  That will be the first time it has been stored inside since she bought it in 2007.

[ Photo 1 of 1 – HC – The large bay of garage ready to accept our Honda Civic for the winter.  This is the first time we have been able to put a car in the garage since we moved in to this house. ]

The large bay of garage ready to accept our Honda Civic for the winter.  This is the first time we have been able to put a car in the garage since we moved in to this house.

The large bay of garage ready to accept our Honda Civic for the winter. This is the first time we have been able to put a car in the garage since we moved in to this house.

We rearranged some things in the front of the smaller garage bay to make room for the large trash container, the wheelbarrow, several 10′ lengths of 1-1/4″ plastic conduit, 10 large paver blocks, and the mower deck for the Cub Cadet lawn tractor.  With those things stowed inside the concrete driveway was now free of objects that Kerry could have hit with his snowplow.

The tractor and 18 cubic foot trailer will remain in the yard alongside the driveway where we park the bus.  The tractor won’t start and we had no interest in pushing it uphill through snow.  We found our large plastic tarp the other day so we unrolled it, covered the tractor and trailer, folded the edges under, and weighed the edges down with landscape blocks.  Hopefully it will stay put through the winter.

With sunny skies and the temperature hovering around 50 degrees F I opened the house electrical bay on the bus.  We loaded the four toolboxes onto a hand truck, two at a time, and rolled them over to the bay where Linda got them stacked and pushed in.  We then loaded the two drill cases in front of the toolboxes and I closed up the bay.

Next we opened the passenger side engine bay door and replaced the main engine air filter.  It did not look that dirty but the new one was obviously very clean by comparison.  This air filter is a bit pricey at $130 plus tax but it is so critical to good engine performance that it does not make sense to try and save a few cents by not replacing it or trying to clean a used one and reuse it.

With the air filter changed we then pulled out the chassis battery tray.  It holds four Group 31 lead acid batteries and is very heavy.  It has a very heavy duty slide out tray but the tray is worn and lets the leading edge drop a little bit as it comes out.  That means we had to lift it as well as push it to get it back in.

We applied a 14″ strip of black Gorilla Tape to the horizontal frame member at the top of the compartment opening to prevent metal tools from coming in contact with the chassis, which is tied to the battery ground.  I got this idea from Chuck when I saw that he had done this to their coach.  There was some fine rust on top of the batteries but the connections were all tight and did not show signs of corrosion.  I should probably have cleaned them anyway but we had too much else to do.  I did notice, however, that one of the batteries was from 2009 and the other three were from 2010 so they may be due to replaced.

I opened the doors on both sides of the front bus bay and climbed in.  Linda carried stuff over from the driveway and the living room (of the house) and I figured out how to fit them into the space.  We have less stuff in the front bay then the last two winters but more stuff in the car.  The problem for the bay is that we have things in open topped cardboard boxes so I could not stack things the way I have in the past.

We were done with this phase of the loading process by 3 PM.  I had turned on the main engine block heater and the Aqua-Hot engine preheat loop at 1 PM.  I started the main engine to air up the suspension, leveled the coach, and then turned on the auxiliary air compressor to maintain it at level.  I was getting ready to pull my car around behind the bus so we could hook it up when I realized I should probably move the bus a little bit first to make sure the brakes were not locked up.  I backed it up a few feet and turn pulled it forward a little farther than where it started.  Linda checked the floor and it was level so I switched the suspension back to Level Low to help minimize leaks and hold the pressure.

I continued to let the bus run on high idle while we hooked up the car.  With all of the connections made I opened the air valve that supplies air to the auxiliary braking system in the car and went to the cockpit to activate the various lights while Linda checked them.  Everything checked out as OK.

With the bus still idling we carried the HP Color LaserJet network printer from my office in the basement upstairs and into the bus.  It was heavy and awkward but we got in into the bus.  I had to remove the center cover from between the desk pedestals and we had to get it into its alcove in the left pedestal from the knee space between the pedestals.  I was pleased, however, that it fit very comfortably in that space as the space was designed to hold this particular printer.

Once the printer was in we found the replacement black toner cartridge and put it on board.  Linda also carried the smaller APC UPS up from the rec room to the bus and I put it on the connector cover shelf.  I think there will also be room on the shelf for one of the NAS units.  The newer one is physically smaller but has more storage capacity and is faster but my plan us to take the larger/older/slower one.

We were done with this phase of the loading process at 4 PM.  Our next task was to replace the screen insert from the front door of the house with the storm door insert.  Linda turned her attention to preparing food for our family gathering tomorrow and I stripped the bed, took all of the laundry to the laundry room, and started a load of whites.

My back was making me aware that I had worked it harder today than it would have liked so I took a few more Ibuprofen and settled in on the sofa with the heater pad.  Juniper found my lap almost immediately and stayed there until just before 6:30 PM when I had to get up for dinner.

Linda heated up a couple of Amy’s curry and rice frozen dinners and served them with the remaining kale/almond/raisin salad.  After dinner Linda started packing non-refrigerated food items in paper grocery bags for moving to the bus.  I brought all of my photography equipment upstairs to repack but left that for later.  I went downstairs and pulled two additional sets of BCM issues plus extra copies of some of the issues in which I have had articles.  I boxed the sets, labeled them, and brought them upstairs.

By the time I replied to a few e-mails it was after 9 PM.  We could have worked until midnight but we had both had enough for the day.  I settled in on the living room sofa with the heater pad on my back.  In spite of wearing a knee brace Linda’s right knee was bothering her all day so she took some Ibuprofen and we both went to bed.  We watched Weather Nation for a while and then went to sleep.

Tomorrow will be a long day but of a different sort.  In the morning we will finish loading the bus and I will check/adjust the pressures in all of the bus and car tires.  We are due at our daughter’s house at noon for Thanksgiving dinner and will probably stay until 7 PM. That evening, after we get home, we will winterize the plumbing in the house and spend the night on the bus in final preparation for our departure for Florida the following morning.

 

2015/11/22 (N) Repackaging

My lower back bothered me all night, so I did not sleep well, but we both got up at 8:15 AM, took showers, and got dressed.  My right lower back seemed to have gotten worse overnight.  I pulled a muscle yesterday and they tend to take quite a while to heal.  Not good.

The view of our rear deck from our dining room the morning after our major snowstorm.  It’s pretty if you don’t have to go outside to pack a bus or drive in it.

The view of our rear deck from our dining room the morning after our major snowstorm. It’s pretty if you don’t have to go outside to pack a bus or drive in it.

According to the National Weather Service newsfeed on The Weather Channel iPad app Howell, Michigan got 16.5 inches of snow from yesterday’s winter storm, the highest in Michigan.  The highest accumulation in the country was 18 inches somewhere in South Dakota, so we were very close to that.  The official amount was no doubt recorded at the Livingston County Airport about 11 miles west of us on the west side of Howell, but based on what we see on our deck we got at least a foot of snow here at the house.  It was sunny but only 25 degrees F when we got up.  The high temperature was forecast to only reach 30 and the low tonight is forecast to be 18.

Linda made vegan pancakes for breakfast.  She cooked blueberries into hers but I had mine on the side.  I think the blueberries add additional liquid to the batter and keep the pancakes from cooking properly, but Linda likes the way they turn out.  I made a pot of coffee with the last of our Ethiopian Yirgacheffe beans.  I took some Ibuprofen along with my usual morning pills.  Linda got the heating pad out and I sat with it against my lower right back on the living room sofa while we drank our coffee.  In spite of having a lot to do between now and Thanksgiving Day, we got a slow start to our day.

Linda cleared our front sidewalk so she could get to the front door of the bus.  She also shoveled a path to my car, which I parked behind the bus yesterday, and cleared the snow off of it.  She checked the snow depth with a ruler at several places on our rear deck.  It was 13 inches.  Not 16.5 inches, but it’s still a lot of snow, and it could certainly have been deeper out in the yard.

Her agenda for the day was to vacuum the inside of all the cabinets in the bus, dust the woodwork, and clean the counters and mirrors.  I exchanged some text messages with Chuck including a couple of photos.  I sent one of our bus buried in snow and he sent one of the palm trees and lush vegetation on the unoccupied lot next to theirs at Pelican Lake Motorcoach Resort.  Chuck said it has been too warm to play golf.  I did not know that was even possible but I did not feel too sorry for him.  I sent an e-mail to Butch to let him know I had delivered the antique SUN Electric distributor tester to Bill a week ago Friday.

I resumed working in the garage and spent most of the day repacking my tool boxes.  My objective was to reduce the number of boxes from five to four while maintaining some sort of reasonable logic to how they were organized.  I took short breaks throughout the day to get off my feet and had a few pretzels with hummus for lunch.

Sometime during the afternoon Kerry showed up and plowed as much of the concrete driveway as he could.  Linda must have been vacuuming in the back of the bus and I was working in the garage (with doors closed) so neither of us realized he was there until after he was gone.

I decided that I needed some additional storage boxes for organizing small parts so I drove to Lowe’s hoping to find the Stanley boxes I already have.  They had similar boxes from a different manufacturer but not the exact ones.  I tried The Home Depot but liked the boxes at Lowe’s better so I went back there and bought six, three with 10 deep bins and three with 17 medium bins.  I stopped at Meijer’s for orange juice and picked up a few other things.

When Linda was done cleaning the bus she started loading the things onboard that she had ready.  She got almost everything on board that was staged in the middle bedroom and the kitchen.  She then made three more batches of granola.  That made nine batches since Friday evening, eight of which are in the freezer.  Linda thinks a batch will last at least two weeks if have granola every other day.  If that proves to be true we should have enough granola with us in the bus to get through the end of March.

By 5:30 PM we were both ready to stop for the day.  I changed into my robe and sat on the living room sofa with the heating pad on my lower right back.  We spent 45 minutes considering possible waypoints between here and Williston, Florida.  We did not come a decision but it is very likely we will stop at two of the same places we used two years ago, the Oh Kentucky campground in Berea, Kentucky and the KOA near Cartersville, Georgia.

The Oh Kentucky RV Park in Berea is just west of I-75 at an interchange.  It wasn’t fancy but provided easy in/out access and would allow us to plug in for the night.  Just east of the Interstate at the same exit is a Walmart where our friends, Chuck and Barbara, stayed on their way south a few weeks ago.  The RV park options north of Atlanta, Georgia are surprisingly limited.  The Cartersville Castle-White KOA is convenient to an exit off of I-75 and also provided easy in/out access.  Staying there Saturday night means we can drive around Atlanta on I-285 on Sunday morning, our favorite time to bypass major cities.

Our final waypoint before going into Williston Crossings on Tuesday, December 1st will probably be Mayo, Florida where we can boondocks for two nights at John Palmer’s place.  This itinerary would have us traveling about 400 miles on Friday, 300 miles on Saturday, 340 miles on Sunday, and 75 miles on Tuesday.  Friday would be a longer drive by about 2 hours than we normally plan, but very doable.  Also, this time of year we like to get as far south as quickly as possible.

Linda opened a bottle of Leelanau Cellars Mixed Berry Winter White wine to have before, during, and after dinner.  For dinner Linda cooked a squash and heated up some frozen corn and mock chicken tenders (vegan).  After dinner I tried to check my e-mail but our Internet connection had slowed to an unusably slow speed.  At 8 PM I participated in the SLAARC Information Net and then came back upstairs and went to bed.  We both took some Tylenol PM at 11:30 and then turned out the lights.

 

2015/11/21 (S) Not Quite As Planned

The weather forecast for today had snow moving into the area starting at 4 AM, increasing in intensity by 8 AM, and continuing through the day and into the evening.  The initial forecast was that we would get 4 – 6 inches of accumulation with temperatures hovering just below freezing.  We overslept this morning and did not get up until 7:30 AM but decided to go to our weekly ham radio club breakfast in South Lyon anyway.  I have had Mike’s (W8XH) climbing harness for a while and wanted to return it before we left for the winter.

There was already some accumulation on grassy areas when we left at 7:45 AM but the drive was not a problem and we arrived at 8:10.  We were the last ones there, of course, but someone had to be.  We had a nice chat with Harvey (AC8NO) and Diane, who are usually close to the last to arrive.  I called Mike, who did not make it to breakfast, and let him know I was transferring the harness to Harvey.

On the drive home we stopped at Meijer’s in Brighton so Linda could get some additional ingredients to make more granola.  By the time we got home at 10:30 the snow was starting to pile up.  I had four text messages from Kristine Gullen in quick succession which turned out to be four parts of one message.  She wanted to pin down our dinner plans for this evening.  I texted her back once I got home and after a couple of exchanges we came to the mutual conclusion that the weather was going to interfere with our get-together.  Sadly, that meant we would not see her and Jim again until May 2016 as they were probably headed to Frankenmuth for the Fall MERA conference and then on north to their cottage at Crystal Mountain for the Thanksgiving holiday.

Snow piling up around the bus less than a week before our planned departure for Florida.

Snow piling up around the bus less than a week before our planned departure for Florida.

Our original plan for today was to clean the inside of the motorcoach and then start cleaning up the garage/shop.  With the snow piling up we decided to defer cleaning the rig and concentrate on cleaning up the garage and staging things that we will eventually load on board.  I worked in the garage most of the day although that included moving things into the library and house.  Linda concentrated on making granola, preparing a billing statement for the bakery, and organizing/staging kitchen-related things for the bus.  She also came out and helped me when I needed assistance.

My objective for today was to get one of the temporary workbenches cleared off and disassembled.  I also wanted to get all of unused plywood stored flat.  By 5:30 PM we had accomplished those two goals, gotten most of the power tools put away, moved quite a few things to the library, and stored or thrown away quite a few other things.  I had also managed to strain my lower right back.  That is never a good thing, but it was especially bad given what we have to accomplish in the next three to four days.  We will continue the process tomorrow and I will try to get my tool boxes reorganized before I quit working for the day.  A critical piece of the cleanup will be getting everything that should be protected from freezing out of the garage and into the library as we do not heat the garage while we are away even though it has a furnace.  From there some of it may get moved to the laundry room in the basement, or not; it just depends on time and energy.

We need to clean up the garage enough to get the Honda Civic inside and also the (non-functioning) lawn tractor.  Optionally we can leave the tractor where it is and put a tarp over it or I can borrow Mike’s trailer and take it to Sloan’s in Linden to have it repaired and stored for the winter.  I like the last option best but I doubt that I will have the time to take it there before we leave.  It would have to be on Wednesday, assuming they are even open the day before Thanksgiving.

Snowstorm in progress.  Lots of snow on the rear deck and still coming down.

Snowstorm in progress. Lots of snow on the rear deck and still coming down.

For dinner, Linda sautéed an onion with some mushrooms and heated some frozen broccoli and peas.  She used all of that as toppings for two baked potatoes.  We watched the snow fall as we ate and estimated the accumulation on the railing of our rear deck to be at least a foot.

By 7 PM Howell had officially recorded 14.5 inches of snow and it was still coming down.  I decided to text Kerry Fear, who does our snowplowing, to let him know that I staked the driveway yesterday but we still have a mower deck, wheelbarrow, paving blocks, and plastic conduit in the northwest corner of the drive that we have not yet had a chance to remove.  He texted back that he was “up north” and would be back Sunday afternoon.

We went to bed before 9 PM, watched a few minutes of weather on TV, and caught a bit of a Cirque du Soleil holiday show on Detroit PBS.  I was going to call Butch and text Chuck but it was after 10 PM so I went to sleep instead.

 

2015/11/19 (R) FTH Annual Meeting

I was up at 7:45 AM and got dressed right away to work.  I folded the towels and blankets I laundered yesterday and then made coffee and had a bowl of granola for breakfast.  I sat in the living room for most of the morning finishing my blog post about yesterday, having decided that I would probably not work in the bus today.  The only thing I really have left to do is install the metal edging where the floor tiles meet the top of the wall tiles in the front passenger platform and secure the old step on the platform.

I finally inventoried my issues of BCM and sent the list to Gary of the ones I need to make three complete sets for door prizes for the Arcadia Rally.  We had some additional e-mails back and forth regarding the rally.

Part of getting ready to leave is getting the house ready for us to be gone.  I shut the off the water to the three outside spigots and then opened them to let them drain.  I added insulation around the top of the foundation in the sump pump closet and put the piece of insulation back in the window.  I topped off the battery for the backup sump pump with distilled water.  I left the light on to act as a heater and put a note on the outside of the door to that effect.  I also noted the date the battery had been topped off. Once the cats are on board the bus we will leave the sump pump closet door open to let heat get in there.

At 3:15 PM I printed off the documents for the FMCA Freethinkers meeting.  I got a bowl of nuts and made a cup of hot tea.  Linda texted me at 3:30 that she was leaving the office.  At 3:55 PM I dialed into the meeting.  Bob, the chapter president and organizer of the teleconference, was already checked in.  By 4:05 we had 11 F#’s represented, exceeding the eight we needed for a quorum, and he called the meeting to order.

The meeting was routine but necessary.  I edited the minutes from last year as the meeting progressed.  We approved the minutes of last year’s annual meeting, presented the financial statements, received the report of the nominating committee, and elected people to the offices of president, vice-president, and Treasurer.  We also elected five members to serve on the nominations committee for the coming year.  The meeting concluded with a discussion about how to let FMCA members know about our chapter, which resulted in a member volunteering to set up a public Facebook page for our chapter.  Linda got home as the meeting was concluding.

We both got comfy in our robes and spent 45 minutes relaxing in the living room.  For dinner Linda made green salads with dried cranberries and slivered almonds and heated up some mock (vegan) riblets in barbecue sauce and some vegan baked beans.  We finished off the bottle of Barefoot Moscato wine for dessert.

I finished editing the minutes of this year’s meeting, converted them to a PDF, uploaded them to our Dropbox, and e-mailed the members.  I got that done before 8 PM so I could relax and watch a few Thursday evening TV programs with Linda.

 

2015/11/18 (W) Fuel Run

Linda was up at 5:45 AM and off to the bakery at 6:15.  I was up at 7:45 AM and skipped breakfast and coffee.  I put on Weather Nation and took stock of the forecast while I folded the clean laundry.  I took a shower, got dressed, made a cup of tea, and had a small glass of orange juice to wash down my pills.

My main objective for today was to get the bus fueled which would also serve as a test run.  The forecast had the chance of rain increasing through the morning and heading towards certainty by early afternoon, albeit intermittent and not very intense.  I wanted to take care of the fueling before the rain settled in but wanted to wait long enough for the temperature to rise so I set 11 AM as my target departure time.  Before I moved the bus, however, several things had to be done.

First on the list was turning on the electric block heater for the main engine.  It wasn’t cold enough for this to be necessary but having the oil warmed up a bit never hurts, especially with the straight 40 weight oil.  It helps the engine crank over and get oil to the bearings more quickly.

The living room and kitchen in the bus looking aft from the cockpit. New flooring, new seating, new desk, new refrigerator, new slide-out pantry, and new window shades (rolled up).

The living room and kitchen in the bus looking aft from the cockpit. New flooring, new seating, new desk, new refrigerator, new slide-out pantry, and new window shades (rolled up).

Next was simply cleaning up the interior so the coach could be safely moved and nothing would get broken.  I gathered up all of the tools and materials that I no longer needed and moved them into the house and garage.  I then installed the solid brass door stop on the bottom of the pull-out pantry.  Finally I mounted the two aluminum angles to the inside of the refrigerator alcove, one by the freezer door and the other by the fresh food door.

The angles were 1/2″x3/4″ with holes drilled in the 3/4″ flange for #6 SR self-drilling wood screws.  I had carefully countersunk (chamfered) each hole so the screw head would be close to flush with the surface of the flange.  The aluminum was only 1/16″ thick so I had to be careful not to overdo it.  With the freezer door open I set the 1/2″ flange against the face of the refrigerator case (on the side opposite the hinges) and held the 3/4″ flange square to the side of the alcove.  I used a #5-6 self-centering VIX drill bit to drill three holes about 3/8″ deep and installed the 5/8″ #6 screws with a manual screwdriver so as not to over torque them.  I repeated the procedure for the second angle which was longer and had five mounting holes.

The new floor in the cockpit of the bus.

The new floor in the cockpit of the bus.

I had a little spare time so I drove my car up and down the new driveway to compact the gravel.  I won’t drive the bus on this new driveway until next year but it already supports the cars very nicely and the weight of the Honda Element was sufficient to knock down some of ridges and compact the surface.

I checked all of the tire pressures and they were OK so I did not have to get out an air compressor and adjust them.  I will have to do this next week before we leave, however, as the temperatures will have cooled off significantly by then.

Around 11 AM I turned on the coach batteries and opened the auxiliary air supply valve for the engine accessories.  I turned off all of the electric heating elements and made sure the inverter was turned on and then started the main engine.  I let it run for one minute and then switched it go high idle.  While the engine was warming up and the air pressure was building I shut off the shorepower, disconnected the power cord, and stowed it.

I pulled out at 11:15 AM and headed for the Mobile Truck Stop at exit 122 on I-96, approximately 22 miles from the house.  While there are a couple of closer places I could get fuel this truck stop has very good egress and is fairly busy, which means the fuel is being turned over frequently and is thus relatively fresh.  The drive is a mix of Interstate and Michigan Highways with a few stoplights and a couple of miles of dirt road, so the bus has to run up and down through its gears.  It is also a long enough round trip to get the engine up to normal operating temperature under load.

I estimated that the tank would take on about 120 gallons of diesel fuel so I added two bottles of Stanadyne Performance Formula and one bottle of Stanadyne Lubricity Formula.  The tank started whistling at 112 gallons, which meant it was getting full.  I added the last few gallons by controlling the flow manually and stopped at 119.990 gallons, so my 120 gallon estimate was pretty good.  I paid for the fuel and got a free beverage to go with it.

I had some occasional light rain on the drive out and on the drive back but the trip was otherwise uneventful.  I was back at 12:45 PM, parked the coach, and started the auxiliary generator, which I had not done for several months.  To load the generator I turned on all three electric toe-kick heaters, the engine block heater, the Aqua-Hot electric heating element, and front bay electric heater.  I let it run for 90 minutes with an average current draw of 25 Amperes on each leg, which is about 35% of its full load capability.

I got the shorepower cord out and connected it but did not turn it on.  As long as I had water and air pressure I flushed the toilet and then ran a little water through the various faucets in the coach.  I set a rubber door mat under the drain for the fresh water tank to keep the water from drilling a hole in the driveway and then let the tank drain slowly.  While it was draining I got the long fresh water hose out and connected it to the spigot on the front of the house and the water port for the coach.  With the fresh water tank empty I checked that the outside water spigot was configured to provide filtered/softened water.  I closed the drain valve, opened the fill valve, and opened the valve at the house.  I then went in the house, set a timer, and had a bite of lunch.

I had a phone call while I was driving back from the truck stop but did not answer it.  The caller left a message so I listened to it and then called him back.  Kevin Stufflebeam, from the southwest part of Michigan, had a 1995 Marathon Prevost conversion with a non-functioning Webasto system.  It turned out that he had the system worked on by a company in that area and the guy from the company had called me during the summer.  They got my name and contact information from Josh Leach at Coach Supply Direct, with my permission.

The fresh water tank has an overflow tube so that is how I knew it was full.  I closed the fill valve on the bus, closed the spigot valve at the house, and then opened the fill valve to relieve the pressure in the hose.  Sure, it was a lot of back-n-forth, but it eliminated the spray that occurs when unscrewing a fitting on a pressurized hose.  It also makes the fitting easier to unscrew.  I removed the hose from the coach and then from the house.  The spigot is about four feet higher than the driveway so I pulled the hose up towards the spigot, allowing it to drain as I coiled it up.  Once it was coiled I connected the two ends together, put it back in its storage tub, and put the tub back in the front bay.

Linda called at 4:30 PM to say she was on her way home.  It had been raining, off and on, all afternoon so I took about 45 minutes to drive on the new driveway with my Honda Element and compact it even more.  But first I got the metal toothed rake and evened out the few remaining ridges and valleys.  Besides going up and down the driveway I drove across it at various angles at both ends.  Most of the driveway has fresh topsoil along both edges, which is soft and has grass seed and straw on top of it, so I stayed off of those areas as they definitely should not be compacted.  The end of the new driveway by the house ties into our concrete driveway and some solid, undisturbed lawn with a flare.  The far end, which ties into the street at our third culvert, is much wider (to allow the bus to make the turn), relatively flat, and ties in to solid, undisturbed lawn.  The concrete, road, and undisturbed lawn allowed me to drive beyond the edges of the driveway in these areas and go across them at various angles.

Any kind of weather always slows commuter traffic and Linda did not get home until 6 PM.  It had been a long day for both of us and she just wanted to relax for a while.  She opened a bottle of Barefoot Moscato and poured each of us a glass.  For dinner we had mock oriental orange chicken with reheated frozen broccoli and white rice with soy sauce.  It was an easy but very tasty meal.

After dinner I finally settled in at my desk to finish updating the FMCA Freethinkers Chapter roster, financial statements, and minutes from the 2014 annual meeting.  Linda reviewed the financial statements and helped me reconcile them to the bank statements.  Once we were satisfied they were accurate I saved everything as PDFs, uploaded them to our Dropbox, and sent the folder link to the members via e-mail.  We then headed to bed and watched the last episode of The Brain on Detroit PBS.  Linda went to sleep and I wrote for a while, finally turning the light out at 11:30 PM.

 

2015/11/16 (M) Tiling the Cockpit, #3

Linda planned to go to the bakery today but decided yesterday to stay home and help me instead.  Based on the 10-day forecast this looks like our last decent weather day to work on the bus and we wanted/needed to make the most of it.

We had breakfast at 8 AM (granola with blueberries and a banana) and had a cup of Stash China Black tea.  I had a text message from Kristine Gullen regarding getting together with her and Jim on Saturday and replied in the affirmative.  We finished our tea by 8:30 and got to work.

I really wanted to finish tiling the cockpit of the bus, or at least as much of it as we could.  That meant cutting and fitting tiles for the stair treads and risers and the two side walls of the entry steps, gluing them in place, and then grouting all of them.  We needed to mount the table if possible and I also needed to build a new step for the platform.  That was a lot to get done in one day and even before we started I doubted that we would get it all done.

When we opened the bus we were surprised to find that the tiles on the walls of the platform had slipped all the way down to the floor tiles.  Obviously I should not have removed the spacers right after installing the tiles and should have to left them in place for any horizontal grout spaces on vertical surfaces.  Oh well, not much to do about it now.

Keith called to see if he should come and mulch the leaves one last time.  The weather the last few days had been very nice, unseasonably warm and dry.  Today was also a beautiful day but the forecast going forward was for much cooler and wetter conditions, so this was an ideal day for our last lawn mowing of the 2015 season.

We measured and cut the tiles for the face of the platform and out to the door.  At that point I evaluated what I needed to do to complete the job.  Basically, I needed to cut all of the tiles for the entry steps and walls and then install them from the bottom up.  Every piece of tile was going to be smaller than a full 16″x 16″ tile and custom cut so even though the square footage was not that much there would be more pieces than usual and it was obviously going to take quite a bit of time to get all of the pieces ready to install.  I thought we could be ready for adhesive in two hours but Linda figured it would be at least three.  It also meant working with the door open which would make it difficult to keep the interior as warm as we needed.

Phil showed up with his excavator and a dozen bales of straw.  I knew the excavator was for a different job as he did not have anything left to do at our place that required it.  He was here to finish covering the topsoil and grass seed with the straw.  We took a break to go talk to him and confirmed that he was done with the driveway and French drain projects except for the straw.  He staged the bales where he needed them but said he had to leave to dig a perk test hole at 1:30 PM and would be back mid-afternoon to finish spreading the straw around.

Linda suggested that we go ahead a grout all of the tile we had already installed.  I was more emotionally invested in completing the tile work than Linda but had to agree that this was the prudent thing to do.  Until the tile was grouted we could not reinstall the accelerator, the steering column shroud, the seat bases, and the seats, so grouting the tile was clearly a critical path item and that is what we did.  It was after noon by the time we finished so we took a break for lunch.  Phil had taken off by this time to go dig the test pit.

Lunch was grilled vegan Italian sausage on a bun with mustard and relish and black grapes on the side.  Keith finished up mowing the yard while we were enjoying a cup of Rooibos tea.  We paid him and chatted about next year.  I gave him our approximate timeframe for returning home from Florida and asked him to go ahead and start mowing next spring whether or not we were here.  We have had Keith take care of our lawn since we bought our house in the country and he has been very good about doing that when we are away and allowing us to catch up with him when we get back.

By the time we got back to work on the bus it was after 1 PM and I had to concede that we were done working on the tile until next spring except for cleaning them, which had to wait until tomorrow as the grout has to cure for 24 hours before final cleaning.  With that decision made we considered what else needed to be done and in what order.

The first order of business was painting the two front seat bases black.  We spread out painter’s plastic on the driveway and taped it down.  We set the bases there and then masked off the top portion with the swivel bearings and mounting bolt.  We wire brushed the bases to remove rust and then went over them with a sanding sponge.  I used a cleaner/degreaser and water to clean them and then gave them a coat of black rubberized undercoating paint.

The next order of business was getting all of the tools and materials that we no longer needed out of the bus to give us room to work on other things.  On Saturday I re-installed the bump out on the walnut cover for the passenger side HVAC duct.  The duct needed to have two 4″ holes drilled in it to match the holes in the metal duct, so that was the next task.  I measured very carefully and transferred the measurements to the face of the cover with equal care.  Even so, I was off slightly and had to use the sheet metal nibbler to enlarge the bottom of each hole.  At least I had a relatively straightforward way to fix this problem; I am not always so lucky.

With the holes enlarged we put the cover in place.  The 4″ round plastic registers fit through the wood into the duct but not all the way due to two tabs.  I trimmed the tabs off using the Porter-Cable oscillating saw and trimmed a little bit off of one of the outer mounting flanges to make it fit flush.  I drilled holes through the two mounting holes on each register using the #5-6 self-centering drill bit and secured them with #6-5/8″ SR screws.  We then removed the two temporary black plastic registers from the front of the built in sofa.  I trimmed the tabs off of two new brown ones and installed them using the same procedure as the first two.

In the grand scheme of things getting the cover in place and the four registers installed was a small task but it needed to be done and stood in the way of other things.  The cover has been stored on top of the two front seats, which have been lying on their backs on the kitchen floor of the bus for weeks.  We plan to re-install the seats late tomorrow afternoon.

Two more small, but critical, tasks were securing the pull-out pantry and the refrigerator.  I have assumed for quite a while that we would secure the pantry for travel with some form of sliding latch but had not thought about it in any detail.  We also needed to secure the refrigerator but I had not thought about this in any detail either.  As we pondered the pantry latch it slowly became obvious that we did not have enough wood for a strike plate to receive a pin and we did not have two unobstructed surfaces that were in the same plane, which would be required for the kind of latch I had been thinking about.

As for the refrigerator, one of our bus nut friends secured their unit by running mounting bolts (machine screws) through the floor of the cabinet above the fridge and threading them into the unused tapped holes provided for the upper door hinge (if it was reversed) .  After looking at it for a while we realized that we could attach a section of small angle to the inside of the right alcove wall with the other side just against the face of the fridge case but not over so far as to interfere with the door gasket.  My measurements indicated that a 1/2″x3/4″ angle would be just right.  It looked to me like two 12″ pieces, one by the freezer door and one by the bottom of the fresh food compartment door, would be more than adequate to keep the refrigerator from rolling out as it cannot shift sideways or twist due to the aluminum angle on the left/hinge side at the floor.

About this time Phil returned in a red pickup truck.  He finished distributing the straw and loaded three unused bales into the back of his truck.  He pulled up in the main drive and we invited him into the bus to see what we had been working on all summer.    It is always a pleasure working with Phil.  If/when we build a barn we will have him do all of the site prep and finish grading.  He will figure out the final cost for the driveway extension and French drain and send us an invoice.

Linda prepared an easy but tasty dinner consisting of a nice green salad, mixed frozen vegetables (corn, peas, and carrots) suitably reheated, and mac-n-cheese that was both dairy-free and gluten-free.  After dinner we went to Lowe’s and The Home Depot.  At Lowe’s we bought a 1/16″ thick 1/2″x 3/4″ aluminum angle and three 8 foot lengths of brass colored nose edging but did not find a latch that we liked.  At The Home Depot we bought some screws for securing the handle on the front of the pull-out pantry and a solid brass door stop to keep the pantry in place.  The door stop folds up when not in use and should work to keep the pantry closed while traveling.

Although the new Panera on the southwest corner of Grand River Avenue and Latson Road was finally open for business we stopped at Teeko’s Coffee and Tea on the northeast corner of that intersection.  Jeff was there and took our order for eight pounds of coffee beans.  We got two pounds each of Ethiopian Yirgacheffe, regular and decaffeinated, the Seattle Blend (regular), and the Sweet Dreams blend (decaffeinated).  They will roast the beans and then let them outgas for a few days before vacuum sealing them in half-pound portions.  This allows us to take them with us in the bus and keep them very fresh until we are ready to use them and to change what we are drinking more often.

We got home just after 8 PM and took our iPads downstairs to use while we watched our Monday evening CBS TV programs.  We caught the weather forecast and then headed to bed.  It looks like we will have two more days with unseasonably high temperatures near 60 degrees F but with intermittent rain and then a serious cooling trend with highs this weekend barely above freezing.  Our time for working on the bus and being in Michigan is definitely running out.

 

2015/11/13 (F) Road Trip

I set my alarm for 5:30 AM and got up when it went off.  I got dressed quietly, fed the cats, refilled their water fountain, and took my allergy pill and B-12 vitamin.  I used a plastic bag to pack a change of underwear and socks, a basic oral hygiene kit, my iPad, my checkbook, and my phone charger cable.  I loaded my travel bag and walnut pieces into the car and then checked the mousetraps in the pantry.  One of them had two mice in it.  It was still pitch dark outside so I drove to the end of the new driveway, parked with my headlights pointing across the road, took the trap to other side of the road, and released them.  They went scurrying off into the thick undergrowth of the woods and I drove back to the house.  I left the trap on the front porch and went inside to wash my hands.

I finally left on my road trip to Indiana at 6:20 AM.  I needed fuel so I headed south on Hacker Road and stopped at the Shell Station on Grand River Avenue at I-96.  There is a Dunkin Donuts co-located with the station so I got an extra-large coffee and was on my way.  I decided to head east a couple of miles on I-96 and then south on US-23 to Ann Arbor where I picked up I-94 west.  I took I-94 as far as I-69 and then headed south.  Somewhere along this segment I realized I had forgotten the box with the two swivel ring bearings.  That meant I would not be stopping at Coach Supply Direct in Edwardsburg, Michigan to return them, which would save me time but necessitate getting them back to Josh another time and/or another way.

The change in plans would loosen up my schedule a bit but I still had four stops to make and was anxious to make time.  I stayed on I-69 south into Indiana and then took the Indiana Toll Road (I-80/90) west.  Traveling west there is one travel plaza between I-69 and the SR-19 exit.  I stopped there to use the restroom and get another cup of coffee.  Back in my car I called Josh to let him know I would not be stopping by his shop today in Edwardsburg.  I then called Linda to update her on my whereabouts and change in plans.  She said she would take care of getting the box with the swivel ring bearings ready to mail.

The weather was overcast, drizzly, cool, and windy when I left this morning.  The winds were out of the west so I had a crosswind or a headwind for the entire trip down.  By the time I reached Indiana I had driven out from under the cloud cover.  The temperature remained very cool but the sunshine was refreshing.

My first stop was A-1 Upholstery in Elkhart, Indiana.  Much to my surprise Terry had used the exact same fabric for the filler cushion that we had her use for all of the other ones, so it was a perfect match!  I got a call from Josh while I was there and called him back as soon as I left, but got his voice mail.

My next stop was at Pat and Vickie Lintners’ house, about three miles from A-1 Upholstery, to pick up a critical accessory piece for the built-in Nutone multi-function kitchen appliance.  We have a functional power base built in to our kitchen counter in the bus but only had the blender attachment.  Vickie gave us a number of other attachments at a rally back in September but many of them required a right angle tower adapter.  She had found the adapter a few weeks after the rally.

From Pat and Vickie’s I backtracked to the main north-south road, went south back over the St. Joseph River, and headed west on Old US-33 (Lincolnway).  I got a call back from Josh and he said to stay on my current road all the way to the Mishawaka bypass and then head south to US-20.  From there I was on familiar road as I headed west to US-31 south.  Michele Henry from Phoenix Paint had called while I was at Pat and Vickie’s and I let it go to voice mail.  I called her back when I was done talking to Josh.  They had both called me with some recent scuttlebutt about a service facility in Elkhart where friends of ours had some major remodeling work done on their vintage bus, but it was also a chance to catch up on things in general and helped pass the time as I drove.

I stopped in Argos for fuel and called Bill Tharpe with an ETA of 12:30 PM.  I then called Jarel to let him know I would be there by 1:30 PM.  Butch had driven me past Bill’s place once some time ago so I had a fairly good understanding of where it was and what it looked like; not that I needed it.  Given the address my Garmin 465T GPS unit took me right to Bill’s place on Mexico Road south of Mexico and north of Peru.  Sounds like I was in Central America.

Bill was outside waiting for me and we unloaded the antique SUN Electric Distributor Tester from my car and into Butch’s truck, which Bill had for the winter.  He was headed to his building in Wabash, where he has a paint booth, to repaint the truck so we did not chat for very long.  Besides, I still had one more stop and it would take at least a couple of hours.

A couple of miles on down Mexico Road I headed west on US-24 towards Logansport and arrived at Jarel Beatty’s cabinet shop at 1 PM.  Jarel was not expecting me until 1:30 so he was in the middle of cutting dados in side panels for a tall cabinet.  When he finished that task he switched to a regular blade in his table saw to work on my pieces.

We selected the most suitable pieces of walnut from among the ones I brought.  He ripped two pieces, one 2″ wide and the other 2-1/16″ wide, and crosscut them to 19-11/16″ long.  He then ran them through his shaper to round off the edges.  He changed the blade on his table saw, reset the depth of cut, and set the fence to cut off the amount of material I had marked with blue painter’s tape on the bump out for the passenger side HVAC duct cover.  With the sawing done he sanded the two new pieces and then sprayed them with a Sherwin-Williams pre-catalyzed lacquer.  He let the first coat dry for 15 minutes and then lightly sanded it with 220 grit paper to knock down tiny bubbles and splatters.  He then applied a second coat.  It was remarkable to see how it changed the appearance of the wood.  Jarel described it as being like “putting water on a rock” and I thought that was an apt description.

After another 15 minutes the pieces were dry enough to be transported without damaging them.  I wrapped things up with Jarel, including finally remembering to get all of my drawings back, and was ready to leave at 3 PM.  The GPS said I would be home by 7 PM, quite a bit earlier than I expected when I left this morning.

I had smooth sailing until I encountered a major traffic jam on I-96 eastbound just east of US-127 on the southeast corner of Lansing, Michigan.  It took 45 minutes to go three miles and I was sitting at about 1/8 tank of fuel.  Ugh.  There turned out to be multi-car accidents in two separate locations about a mile apart plus a car stopped in the right lane that appeared to have run out of fuel.  What a mess.

Once I was clear of the accident area it was clear sailing once again.  I stopped at the Marathon station at the Fowlerville exit (#127) for fuel and checked out the truck pumps.  Although there were lots of semi’s parked there for the night I was disappointed to find that the back lot was in as bad a shape as the Mobil Truck Stop at exit 117.  Still, the round trip from our house would be 20 minutes shorter and it was an alternative place to get fuel.  The closest place to our house where we can fuel the bus is actually the Marathon station on Grand River Avenue at I-96 in Brighton, which has truck pumps around back, but we have some low branches in the southbound lane of Hacker Road just before we get to Grand River Avenue, so we tend to avoid that route and that stretch of Grand River Avenue is often very busy and not someplace I want to be with the bus unless it is later at night.

I checked the mousetrap in the pantry when I got home and we had caught yet another mouse.  I unloaded the car and then took the mouse trap to the end of the new driveway and released it across the road as I had done with the previous four.  As I walked down the driveway it was obvious that Phil had been here with his bulldozer, which Linda confirmed over dinner.

The “parking pad” area is now presumably level but it was definitely not flat as it had deep marks from the bulldozer treads and ridges where the gravel had not been completely smoothed out.  The top inch or so also seemed very loose.  I don’t think Phil is done working on the project as he still needs to spread straw over all of the topsoil that he placed, graded, and seeded the other day.  I suspect that he still needs to compact the gravel one last time with his track loader but I won’t know for sure until I can talk to him.

Dinner was chili and crackers; simple but delicious.  It had been a long day but I had taken care of four things in one trip, three of which were directly related to the bus and two of those of a somewhat critical nature.  We were both off to bed not long after dinner.  Tomorrow was our weekly ham radio breakfast so we would have to be up early to get there on time.

 

2015/11/11 (W) Two for One

We had late morning dentist/hygiene appointments today so Linda did not get up early to go to the bakery and we slept in and got up at 8:30 AM.  We showered and dressed and finally had granola for breakfast at 9:15.  She made this batch of granola yesterday and it was very yummy.

Since the mice have recently been defeating our simple live traps I cleaned our more complicated one yesterday and set it up last night with a broken open peanut butter pretzel for bait.  When I checked the trap this morning it had two brown field mice inside.  They were anxious to get out and I was glad to oblige.  I set them free in the southwest part of our property on the other side of the road.  The last I saw of them they were headed south into dense cover and away from the house.

Our appointments were at 11 AM in Dearborn.  Linda left at 9:45 and I followed about five minutes later.  We took separate cars since she had to go to the bakery following her appointment.  Before I left I checked on the state of charge of the house batteries in the bus.  There were at 95% SOC.  I turned the charger off last night to let the battery bank drain down a little.  I turned off the Broan cube heater and the three toe-kick heaters and then shutoff the AC power coming into the coach.  I checked that the inverter was working, which it was, and left for my appointment.

We both had good checkups but Linda will need a crown in the spring.  A tooth with an old filling had weakened and needs to be capped.  The dental assistants/hygienists have started taking blood pressure readings as part of modern dentistry’s role in monitoring and promoting overall health.  I don’t know how accurate the wrist cuff machines are but my blood pressure was 121/59 and Linda’s was 128/67, which are excellent readings if they are even close to being correct.

On the way home I stopped at the new Menard’s on Wixom Road just north of I-96.  I was looking for 1/2×2″ fine thread carriage bolts but all they had were coarse thread in longer lengths.  As long as I was there I picked up a 6-pack of work socks and two more of the good live traps like the one we already have.

Back at the house I called Terry at A-1 Upholstery to confirm that our spacer cushion for the bus sofa was ready and that she would be there Friday morning.  Her response was affirmative on both counts.  I then called Josh to verify that he would be at his shop on Friday morning and he said he would.  I need to stop there on the way to A-1 Upholstery and return two swivel seat ring bearings.

The new gravel driveway extension and RV parking pad.  Phil, on the left side of the driveway by the nearer utility pole, rakes out the topsoil he placed along both sides of the driveway.

The new gravel driveway extension and RV parking pad. Phil, on the left side of the driveway by the nearer utility pole, rakes out the topsoil he placed along both sides of the driveway.

Philip Jarrell from Precision Grading was here working on the driveway extension when I got home.  After my phone calls I changed into my work clothes and went out to chat with him for a few minutes.  Phil had brought another load of screened topsoil and was using his track loader to place it along the sides of the driveway extension and at the west end of the property where the French drain begins.  He rough graded it with the track loader and then raked it out by hand and spread grass seed.  He will bring straw bales with him on a subsequent trip to cover the soil/seed but he wanted to get the seed down before he left as we have rain and wind forecast starting late this evening and through tomorrow into Friday.

I finally got to work in the bus at 2 PM.  My objective was to get the SurePly underlayment installed on the passenger seat platform floor.  I lightly sanded the floor patch compound I spread around last night and vacuumed up the particles.  I then mounted the head of each of the new carriage bolts to a thick plastic washer using 3M Heavy Duty (double-sided) Mounting Tape.  I slid the heads into the two mounting channels with the washers under them so the washers held the bolts up off of the bottom of the channel and forced the square collars up in the open slot of the channel where they could not turn when a nut was tightened on them.  This was a critical step because once the underlayment and tile are down I will not be able to get to the heads of these bolts.

With the bolts in position I got the piece of SurePly from the garage.  I was starting to slip it into position when I remembered that I installed an angle bracket yesterday but had not cut out a small piece of the underlayment to fit around it.  So I took the piece back to the garage, cut out the necessary space, and took it back to the coach.  I am starting to wonder how many hours I would have saved by having a proper shop set up right outside the front door of the bus.

[ Photo 2 of 2 – HR – The SurePly underlayment on the co-pilot/navigator platform floor showing how it fits under the outside wall panel and over the four mounting bolts for the seat. ]

The SurePly underlayment on the co-pilot/navigator platform floor showing how it fits under the outside wall panel and over the four mounting bolts for the seat.

The SurePly underlayment on the co-pilot/navigator platform floor showing how it fits under the outside wall panel and over the four mounting bolts for the seat.

The underlayment slipped under the switch panel by the outside wall and dropped over the four mounting bolts just like I planned it, so taking most of yesterday to carefully cut and drill the piece paid off in the end.  That felt good, especially in comparison to how yesterday felt.

The weather today was lovely, reaching a high of 58 degrees F with sunny skies and I am sure that added to by general sense of well-being.  Our part of Michigan is under a high wind warning starting this evening, however, with maximum gusts of 55 to 60 MPH possible.  It’s a good thing we have a whole house generator because those kinds of winds cause power outages.

I decided to screw the underlayment to the bus floor rather than use staples.  Again, I did not want to get the big air-compressor and staple gun out, but I also wanted to use the screws to pull the underlayment down tight to the bus sub-floor.  I was about 50% done when I saw that Phil was putting his track loader back on the trailer.  I thought he was packing up to leave so I went out to talk to him briefly.  I went back to the bus and got another 25% of the piece screwed down before I ran out of screws.  I was using primarily 1″ #6-SR self-drilling screws with some 1-1/4″ of the same kind.  Once again my work was halted short of completion by the lack of some small part.

Phil was finished and on his way at 4:15 PM and by 4:30 I was headed to Lowe’s.  Linda texted me that she was leaving the bakery and I had a nice QSO with Tom (K8TAF) while running my errand.  Lowe’s only had one pack of the 1″ screws, quantity 100, but I thought that might be enough to get me through tomorrow.  I also bought a pack of 100 1-1/4″ screws.

For dinner Linda cooked a couple of yams, heated up a couple of vegan sausages with sautéed onions and red peppers, and steamed some fresh green beans. Yum, yum, yum.  After dinner we sat in the living room for a while using our iPads.  At 8 PM we watched a few nature and science programs on PBS.  Jarel called to confirm when I was coming down to Logansport, Indiana and said that Friday would work.  Linda is headed back to the bakery in the morning so she went right to sleep after we were done watching TV.

 

2015/11/09 (M) Clever Mouse

Madeline coughed quite a bit last night and we were up several times to check on her, so we did not have the best possible night’s sleep.  We got up to stay at 7:30 AM and Madeline got up about 15 minutes later.  I made our morning coffee while Madeline helped her grandma wash blueberries and make vegan blueberry pancakes.  We had a lovely breakfast with orange juice, pancakes with real maple syrup, and blueberries, raspberries, and bananas on the side.

I check the mouse traps in the pantry every morning.  A couple of days ago I found one of them broken with the food gone and some mouse poop left in its place.  The pantry doors had been left open overnight so I figured one of the cats had discovered the trap (we use live traps) and tossed it around until the door fell open and the mouse escaped.  I threw it away since it was broken.  This morning I discovered that the food in the other trap had been replaced by mouse poop but the trap was upright with the door closed and was not broken.  The pantry had been closed all night so I knew the cats had nothing to do with it.  Apparently we have a mouse that has figured out how to defeat the traps.  We are not going to set kill traps so we will have to see what else we can find.

We lingered in the living room for a while enjoying our coffee by the fireplace, listening to Madeline play (with) the organ, and watching her play with some of her toys.  She made her futon into a car and took her two “bunnies” for a ride.  By 9:30 AM I had finished my coffee and changed into my work clothes.  It was just below freezing when we got up this morning, but it was a bright, sunny day with no wind, so it would be a comfortable enough day for working on the bus once I turned up the thermostats and warmed up the interior a bit.

My focus today was to get the SurePly underlayment installed on the floor of the passenger seat platform and maybe the two walls.  I also wanted to get the outside wall panel trimmed off so it will fit around the tile and needed to build a new step with an open front, but I did not expect to get to those tasks today.  First up, however, was getting the small patch I worked on yesterday to fit better and be secure.

I trimmed both ends of the underside of the main patch and recut the side/support panel.  I trimmed the side panel several times before I was satisfied with the fit.  I used heavy-duty double-sided tape to hold the top patch and side panel to the metal structure underneath.  I used a 1-1/2″ stainless steel self-drilling wood screw to secure the top to the vertical piece of 3/4″ plywood that forms the face of the passenger seat platform, and a shorter screw to secure the side panel to the same piece of plywood.  I then attached a temporary plate of SurePly over the side panel to the edge of the top plate to hold the side in alignment with the top.

The metal under this patch is rounded leaving a small space between the top and side pieces where they meet.  The vertical plywood front face is also beveled leaving a void.  I used Door and Window Trim Spray Foam Insulation to fill these areas.  This foam has a lower expansion than most spray foam insulation.  I did not overfill the voids but put enough in that it expanded out past the edge.  I will trim it off flush tomorrow when it is cured.  The foam adheres to anything it touches and is rigid enough to be somewhat structural so it should stabilize and secure the patch.  Once I trim it and cover it with underlayment it should be good as new.

Madeline’s Aunt Meghan, who is also her buddy, came to visit and play with her today.  She arrived at noon and I took a break to visit and have lunch.  After lunch Madeline, Meghan, and Linda went to the Brighton Mill Pond Playscape and I resumed working on the bus.  They were gone for several hours.

Floor patching compound being applied to the co-pilot/navigator platform.

Floor patching compound being applied to the co-pilot/navigator platform.

Before I could put a layer of underlayment on the passenger seat platform I needed to use floor patching compound to fill in some low spots and create a smooth taper from the plywood to some metal edging.  But first I removed all of the screws that secure this edging and counter-bored the holes so the screw heads would be flush.  As often seems to happen when I am working on something like this some of the screws were rusted and I did not have appropriate replacements.  I then have to make a trip to Lowe’s, which is what I did, and bought a small quantity of three different size flathead wood screws.  I stopped at O’Reilly’s Auto Parts to see if they had the large metal or nylon washers that are used with the swivel base for the front chairs.  They didn’t, but once again suggested that I try Howell Hardware in downtown Howell.  I have received that suggestion from people at several different stores so guess I need to check the place out.

When I got back home I finished installing the new screws.  The floor patch compound takes a minimum of three to four hours to dry, sometimes much longer, but after two hours it was dry enough for me to use a sanding sponge to smooth out some ridges and feather some edges that needed it.  It was clear, however, that I wasn’t going to be able to accomplish what I set out to do today.  And so it goes; I need to do the work correctly which means doing all the things that need to be done in the order that they need to occur.  Everything takes time and things that have to dry, set, or cure do so on their own schedule, not mine.

Phil had shown up around 3 PM so I went out to chat briefly with him and then went inside to change clothes.  He had a partial load of topsoil left from a job earlier today and dumped it on the other side of the street by the 3rd driveway culvert.  He used his front loader to place it along the south side of the new pull-through driveway extension and moved the small pile from the west end of the property to the north side of the driveway.

I still had plenty of daylight and wanted to make some good use of my time so I started thinking ahead to the layout of the tile in the cockpit.  I measured various parts of the cockpit and although the number of square feet is small compared to the main floor the layout will be more difficult.  As with all tile layouts it needs to be “balanced” while avoiding small pieces.  Linda and I agreed that the pattern in the cockpit does not need to match the main floor, which is laid out diagonally, so that opens up options for how to lay out the tile.

The main landing is less than two tiles wide (front-to-back) so the best layout for that area is with a grout line dividing it in half, but that might not work well in the driver’s area.  The driver’s area presents the additional problem of a steering column, brake pedal/valve, an accelerator pedal with its electrical cable that goes through the floor.  The “holes” in the tile to accommodate these things have to be created using two notched pieces so they can be installed around the protrusions.  I also need holes for the seat base mounting bolts and power cable for the 6-way power base.  Those can be actual holes but I do not want grout lines to fall at the edges of the base.  I also have to be cognizant of the walls, which are getting tiled.  The distance along the face of the passenger seat platform is close to 65″.  The tiles are 16″ squares so four tiles with three 1/8th” grout spaces is only 64-3/8″.  See, it’s complicated.

The other thing I pondered and measured was the new step between the passenger seat platform and the main floor.  Again there are several parameters:  (1) We want the finished (tiled) height to split the distance from the tiled platform to the tiled main floor exactly in half; (2) we want the finished depth to be half the finished depth of the platform, and; (3) we want an open front so we can store shoes under the step.  The total rise will be just under 14″ so the step rise will be a little less than 7″.  Subtracting about an inch for wood and tile will leave a 6″ high space for shoes.  The platform is 29″ deep so splitting that in half results in two treads of 14-1/2″, plenty deep for shoe storage.  I considered having the step angle across the platform, being deeper by the driver seat and shallower by the passenger seat.  While it would add an element of aesthetic interest it would greatly complicate the construction without adding any practical utility, so I rejected that idea.

As I considered the construction of the new step I was also thinking about the fact that there is a hole in the front end of the passenger side HVAC duct.  The hole opens into the space behind the switch panel on the wall next to the passenger seat and just aft of the entry door but there is nowhere for the air to go from there.  The hole is easy to see but not easy to reach so I estimated it to be three inches in diameter which is approximately seven square inches in area.

One possibility is to install a 4″ diameter circular louvered duct in the switch panel.  It would be large enough in area, could be rotated to direct the flow in any desired direction, and has internal shutters that could be closed down to reduce or cut off the air flow.  The main downside is lack of space behind the panel but I could cut off the tube behind the locking tabs.  Another downside is that the cats sleep under the passenger chair while the bus is moving and the direct airflow might be uncomfortable and/or annoying for them.

Another possibility is to create a narrow duct along the back wall of the platform the same height as the new step and tie it in to the inside of the step, allowing the conditioned air to come out the open front.  That will involve a bit more woodworking and complicate the tile installation, but could be added later, so I will probably opt for the round louvered register for now, if I do anything.

When I was done pondering the HVAC possibilities I put the seat pedestals back on the landing, locked up the bus, and went inside to change clothes.  Meghan left while I was changing clothes so I did not get to say goodbye.  Apparently Linda thought I was taking a shower and would be a while.  Since we needed to get Madeline back to her house well before her bedtime we decided to head to Ann Arbor and have dinner there.  I deflated and rolled up her portable toddler bed while Linda and Madeline gathered up her clothes, books, toys, and other things.  I loaded the car while Linda got her dressed to travel.  I checked in with Phil to get a status update and let him know we were leaving.  We were on our way at 4:45 PM.

The drive down was OK as the really heavy traffic was headed north out of Ann Arbor.  We tried to keep Madeline awake by reviewing all the fun things she had done since she got to our house late Friday afternoon but we were not successful.  As I exited M-14 eastbound onto US-23 southbound I could see that traffic was stopped not far after the Plymouth Road exit so I left the highway and headed west on Plymouth Road to Huron Parkway.  From there I headed south, paralleling US-23 to the west.  At Washtenaw Avenue I turned east, and after a short distance turned left into the small shopping plaza where Elevation Burger was located.

I order a grilled cheese sandwich and Mandarin oranges for Madeline.  Linda and I had vegan burgers and fries and Linda shared her fries with Ms. M.  Madeline was slow to wake up but perked up when her food arrived.  That girl likes to eat!  🙂  After dinner we made the short trip to Madeline’s house and arrived at 6:30 PM.  Linda got Madeline into her pajamas while I brought all of the stuff in from the car and turned up the thermostat.

Madeline was wide awake and full of energy so she played with her kitchen toys and tools and had Grandma Linda read her four stories.  I dozed off for a little while and then spent some quality time with Gus the cat.  Gus loves people but tends to keep his distance from Madeline who is just a bit too energetic and enthusiastic for him.

Brendan and Shawna’s flight was due in to Metro Airport at 6:50 PM and he texted Linda at 6:51 that they had landed.  They were home before 8 PM and got to spend time with their very awake, excited, and active daughter.  We left at 8:30 and stopped at Biggby Coffee on Washtenaw Avenue.  Rain was moving into our area from the south but had not yet arrived and the drive home was uneventful.  We were home by 9:15 PM and headed straight to bed where we watched Scorpion and NCIS-LA.  Linda came down with a cold while Madeline was here and went to sleep as soon as NCIS was over.  I watched Travelscope on the Create channel and left the TV on while I worked on this post.  It was another long, busy day during which I made forward progress on the bus.

 

2015/11/05 (R) POR-15

Linda was back at the bakery today, so she was up early and gone before I even thought about getting out of bed.  Having her homemade granola as our standard breakfast means I can feed myself under such circumstances with very little time spent on preparation and cleanup.  I made a cup of Stash China Black tea instead of coffee; it’s quicker and cleaner.  I like tea, and only started drinking coffee at age 50, but this morning the choice was motivated by ease and quickness of preparation and minimal cleanup as I was anxious to get busy working on the bus.

My focus today was getting the areas in the cockpit where I cut out the old water-damaged plywood ready for the installation of new wood.  That meant getting POR-15 applied to the areas of rusted metal in the cockpit and spray painting over it with black rubberized undercoating paint.  I also wanted to start cutting and fitting the wood pieces that I will use to patch the floor.  I finished building a pair of sawhorses and set them up in the driveway just outside the large garage door so I could measure, mark, and cut wood at waist height.  I was working on one of the pieces when the whole house generator came on at noon, ran its exercise cycle, and shut down 20 minutes later.  Shortly thereafter I heard the rumble of a big truck coming down the road and a few seconds after that Phil’s truck and trailer drove past.

Phil drove to the west end of the property, turned around, and parked down there.  He brought his Takeuchi front loader and used it to spread the large pile of topsoil around the part of our yard where the French drain starts.  He filled in low spots and graded everything off to blend in nicely.  He then worked his way up the drain line towards the culvert that goes under the road.  When Phil was done moving dirt around he spread grass seed and loosely distributed three bales of straw.  That gave him a good idea of how much more straw he would need.

I eventually took a break and walked down to chat with him in the middle of all that work.  He finished moving some dirt and also took a break for lunch.  He will have a load of screened topsoil delivered as soon as he can to use on both sides of the new gravel driveway.  He also clarified that the 40 foot parking pad portion of the driveway is probably not flat/level as it is not finished yet.  When he places and grades the topsoil his equipment will tear up the driveway a bit.  He will then use his bulldozer to finish the driveway, making sure the pad is flat and level.  That was a relief as I thought he was done and I was fairly certain the pad was not flat or level.

By 2:30 PM I finally had the areas of rusted metal prepared and masked off with painter’s plastic.  I applied the POR-15 with a foam brush.  In spite of being careful I got some on my hands and in retrospect should have worn disposable gloves.  The only way to get this product off of things, including skin, is with the POR-15 solvent, which I had failed to purchase.  Once dry it is permanent, so my right hand is going to look like I just changed the oil on the bus until the old skin gets replaced with new.  The drying time for the POR-15 is 2 to 6 hours.  The afternoon high temperature was 72 degrees F so I figured I would check at 4:30 PM.  The directions said I could paint it while it was still tacky as long as it set enough not to transfer.

Linda got home around 3:30 PM and changed into her work clothes.  Phil was still here working but we left him alone.  The weather forecast for overnight and into tomorrow was for rain, possibly heavy, so we did not want to cause any delay in Phil’s work.  I had cut and fit four pieces of wood earlier.  We put painter’s plastic over the sawhorses and laid them out bottom sides up.  Linda put 2×4 blocks under them to get the edges off of the plastic and I coated them with Thompson’s Water Seal.  I am doing what I can to protect this new wood from water damage.

I needed to finish masking off the cockpit with painter’s plastic before spraying the black rubberized undercoating paint so Linda helped me with that.  The plastic is very thin and much easier to handle with two people.  While we were doing that Phil drove past.  We took a break and walked down to west end of the property to see what Phil had accomplished today.  Back in the bus we had the area masked off to my satisfaction by 4:45 PM.

The base of my thumbs were bothering me (arthritis) so Linda shook the paint can for the required three minutes.  Although the light was fading due to the hour of the day and the cloud cover, I was still able to see well enough to spray the paint where needed.  That was the end of our work for the day, except for cleaning up, and I was satisfied with what we had accomplished.  We put some painter’s tape over three areas where we thought water might be getting in and then started putting everything away.

The wood pieces we treated with Thompson’s Water Seal were still wet so I picked them up from underneath and carried them into the back of the garage.  Linda brought the blocks in and set them on the floor and I put the pieces back on top of the blocks.  The directions said to allow at least 48 hours for drying but I plan to flip them over and coat the other side tomorrow if possible.  We are running out of time and I cannot wait two days to seal the other side and then another two days for it to dry.  We put the various tools away, removed the plastic from the sawhorses, and moved the 2×4 stringers and the sawhorses into the small garage bay.  It was 5:45 PM when we closed up the garage and it was getting dark, a clear reminder that summer was behind us and winter was approaching.

We relaxed for a while before dinner.  Linda made a nice salad and reheated the whole wheat linguini she made the other night.  We opened the bottle of Frey Natural White wine to try it.  I liked it even less than their Natural Red, if that’s possible.  It was very dry and since I do not care for dry wines I was not able to judge its other qualities.  Linda did not care for it either, and she tends to be OK with dry wines, so I suspect it is just not a very good wine.  I suggested she find a recipe that calls for white wine and use the rest of it in the dish.

One of our favorite TV shows is The Big Bang Theory.  It has moved to Thursday evenings this season, so we went downstairs to watch it.  The problem is that once we are in front of the TV set we tend to stay there.  I use the time to multi-task and work on my blog post for the day, so it’s not a complete waste of time.  Besides, we do not consider being entertained a waste of our time.  I am enjoying working on the bus, and although some aspects of the work appear humorous in retrospect, I am rarely laughing while in the middle of it.  I like things that make me laugh, and The Big Bang Theory is a very cleverly written show that is well acted and very funny.

 

2015/11/04 (W) Southbound Liberty

Linda decided last night to work at home today rather than driving into the bakery in Hamtramck.  That meant she did not have to get up at 5:45 AM.  She was up just before 7 and I was up just after that.  I made a large pot of Sweet Seattle Dreams half-caffe coffee and Linda toasted slices of cinnamon raisin bread for breakfast.  After breakfast she settled in to work at her desk while I tended to several chores.

I last changed our whole house water filter in May (of this year) and it looked like it was overdue for replacement.  I had one filter element left so I used it.  The process is simple enough:  I turned off the well pump, shut off the valves on either side of the filter housing, released the pressure in the housing, and unscrew the removable bowl.  When I unwrapped the filter and read the directions I was reminded that I am supposed to clean the bowl with warm, soapy water, rinse it clean, and then sanitize it with a bleach solution and rinse it out again.  That requires water, of course, but I had the water shut off and the filter housing disassembled so I had n way to turn the water back on.  The only way to accomplish this would be to stage the needed water before shutting off the water system but I never remember to open the new filter element are read the directions before I start.  I mean, really, it’s not the sort of procedure that requires me to read the directions each time.

One of the old swivel bearings (L) and one of the new swivel bearings (R).  The new one is obviously smaller than the old one and was not compatible with our pedestals and power bases.

One of the old swivel bearings (L) and one of the new swivel bearings (R). The new one is obviously smaller than the old one and was not compatible with our pedestals and power bases.

Not having any running water I wiped out the bowl with paper towels as best I could.  The directions called for lubricating the main O-ring with silicon grease.  I knew I had some from the last time I changed the filter.  It was hiding in plain sight but took me a while to find.  After greasing the gasket and installing it back on the bowl, I put in the new filter element and screwed the bowl back into the filter head, tightening it with the filter wrench.  I turned the well pump back on, opened the inlet and outlet valves for the filter, and let the trapped air out with the purge valve.

Our filter housing takes a larger than usual element.  It is 10″ long, which is the most common length, but 5″ in diameter, which is much bigger than usual.  It’s a dual density spun polypropylene material with a 50 micron nominal rating at the large outside surface and a 5 micron nominal rating towards the smaller core.  These filter elements are not available at the local home stores so I get them from Adam’s Well Drilling and Water Treatment, who installed out current water treatment system.

I gathered up the laundry and put a load in the washer.  I took the label from the new filter element and headed out on an errand run.  My first stop was Adam’s where I bought four filter elements and two bottles of chlorine tablets for the taste and odor portion of our water treatment system.  Wilson Marine is located next door to Adam’s so I stopped there to see if they sold marine grade plywood.  They didn’t but I had a good chat with the associate.  He suggested that for patching the floor in the bus I just use treated plywood or use Thompson’s Water Seal to treat whatever wood I use.

One of the new swivel bearings on top of one of the old swivel bearings clearly showing that the new bearing is small in diameter, inside and out, than the old one.

One of the new swivel bearings on top of one of the old swivel bearings clearly showing that the new bearing is small in diameter, inside and out, than the old one.

My last stop was O’Reilly’s Auto Parts.  Their parking lot was finally open so I could park near the door.  Ronald had me load the containers of used oil and the bag of filters into a shopping cart.  The bag had leaked onto the paper towels I put under it in the back of my car so Ron gave me a cardboard box to put it in.  He simply put the bag of filters in a container but he emptied the six containers of oil and gave them back to me.  They recycle oil but not the containers.

When I got home Linda checked to see if we could take the plastic oil bottles to Recycle Livingston.  Used motor oil is considered hazardous waste and anything that has had used motor oil in it is considered a hazardous material so we could not take the containers there.  I helped Linda load all of the other recyclables into my car and she made a run to the recycling center, the first in a few weeks.  After moving the laundry from the washer to the dryer and putting another load in the washer I got back to work on the bus floor.

 The area behind the panel to the right of the co-pilot/navigator seat.  The mouse nest is gone and the damaged wood has been removed from between the side-to-side seat mounting rails.

The area behind the panel to the right of the co-pilot/navigator seat. The mouse nest is gone and the damaged wood has been removed from between the side-to-side seat mounting rails.

I spent most of the afternoon working on the floor under the front passenger seat.  First I removed the blocking that provides support for the bottom edge of the switch panel but also spans the three floor boards.  I cleaned out the mouse nest behind the switch panel and found the skeleton of a small mouse.  I then got the piece of wood between the mounting channels out.  The drain line for the front CruiseAir evaporator went through this floor near the outside edge but the floor was rotted enough that I was able to break out the wood on the back side and pull the board out.  As I did this I was reminded, once again, about how much of this conversion was built with the idea that it would never have to be disassembled.

I took a break for lunch, which was leftover lentils and quinoa pilaf with some fresh fruit.  After lunch I resumed working on the floor under the front passenger seat in the bus.  I managed to remove most of the rusted metal filler plate.  I made a lucky guess as to where my wire brush was stored and used it to clean the surface of the rusted metal that remained.  I played with different combinations of wood thicknesses and pondered how I will rebuild this area.  I then sprayed the rusted areas with POR-15 cleaner/degreaser and scrubbed them with a sponge soaked in hot water.

I moved to the driver’s seat area and repeated the process.  There was one area with damaged wood that I still had to deal with.  There was an edge about 10 inches long capped with two thin gage metal angles that were badly rusted.  I removed as much of the angles as I could.  I cut off a strip of wood about 2″ wide and 10″ long and removed the rest of the angles.  I wire brushed the area but left the POR-15 cleaner/degreaser for tomorrow.  In anticipation of applying the POR-15 tomorrow and coating it with black spray on rubberized undercoating paint I began masking off the area with painter’s plastic.

For dinner Linda made a salad, roasted eggplant with garlic and breadcrumbs, and mock fish with vegan tartar sauce.  We finished the Frey Natural Red wine with our meal.  I would love to support this company but this wine is too dry for my pallet.

PBS had an interesting lineup of shows this evening on continental formation, natural wonders, and the human brain.  I dealt with e-mail before the shows and we turned in after the last one.  Chuck and Barbara were planning on leaving this morning, southbound for Florida in their 1993 H3-40 Liberty motorcoach.  I did not have any messages from Chuck today so I presume they got away as planned.  They bought a lot at the Pelican Lake Luxury Motorcoach Resort in Naples where they have spent the last six winters and that is where they are headed.  We will be staying about 90 minutes north of there in January and February and will get together with them as time and commitments permit.  We are looking forward to seeing their lot; it has a coach house and they are doing some landscaping, including large palm trees.

 

2015/11/03 (T) The Penultimate Cut

I heard noises in the kitchen at 7 AM and thought the cats might be up to something.  I got up and discovered that Linda was just leaving the house.  She is normally out the door between 6:15 and 6:30 AM but did not set her iPad alarm last night.  I stuck my head out the door and said “good morning” as she was getting in the car.

I had my usual breakfast of granola with fresh blueberries and brewed a half pot of Sumatra Mandheling half-caffe coffee.  I was enjoying my cup-a-joe by the fireplace when Linda called to let me know there was a story coming up on Michigan Radio (WUOM) at 8:30 AM about an underground landfill fire in Bridgeton, Missouri.  Bridgeton is where my sister, niece, future nephew, and grand-niece live and I had just heard about this fire for the first time on Sunday evening while talking with my sister.

I got the leaf blower out at 10 AM and spent a couple of hours blowing as many leaves out from under bushes and away from the house into the yard as I could.  Keith arrived at 10:30 AM and followed his usual mowing pattern starting with the west half of the property.  The lawn in the immediate vicinity of the house is the last area he cuts which gave me enough time to get the leaves out into the yard where Keith could mulch them.

Most of our trees have dropped most of their leaves by now and Keith’s mower did a pretty good job of mulching most of them.  Before he left we discussed having him come back one more time.  The grass has quit growing so my preference is to wait two weeks but that will depend on the weather.  Keith will check with us next Monday and we will decide what to do at that time.

Mike (W8XH) is planning to come over tomorrow after breakfast and help me work on the tower and our Hi-Q 6-80 antenna.  I have been collecting materials that I need and took a little time to see if they would work with the tower.  I also took the Diamond X-300N antenna down as I planned to put it on the tower in place of the X-50N that is currently up there.  My materials were not working quite the way I had hoped they would so I headed to Lowe’s to see what else I could find.  I also planned to drop off the used oil and filters from the bus at O’Reilly’s Auto Parts store.

At Lowe’s I found clamp sets designed for mounting antenna masts and bought a pair.  O’Reilly’s parking lot was still closed off.  It looked like it had been re-blacktopped and they were painting the stripes for the parking spaces.  This was my second attempt to get rid of the waste from yesterday’s bus maintenance.  I will try again tomorrow; with any luck the third time will be the charm.damage

The area beneath the co-pilot/navigator seat.  Not a pretty sight, especially when racing against the clock to get the coach finished for the upcoming winter season.

The area beneath the co-pilot/navigator seat. Not a pretty sight, especially when racing against the clock to get the coach finished for the upcoming winter season.

I finally got back to work on the bus at 2:30 PM and removed the front passenger chair pedestal base.  The entire area under the base, between the side-to-side seat mounting channels, was rotten so I cut out the water-damaged wood.  Just below the wood I found rusted metal which appeared to be delaminating.  Metal does not do that so I presume there was a layer of sheet metal on top of a metal housing.  The main structure of the bus is welded stainless steel but mild steel was obviously used to create compartments.  Ugh.

After cutting out the damaged wood the remaining piece towards the outside was loose but would not come out.  I removed a couple of screws from the 1/4″ walnut veneer side panel and pried the top out with a small screwdriver.  This panel has a lot of switches mounted in it and a lot of wires behind it so I could only pull it out about four inches.  That was enough to see a 3/4″x3/4″ piece of blocking screwed to the floor to catch/secure the bottom edge of the panel.  It also enough to see a very large nest made of tiny bits of shredded paper.

The cavity behind the panel to the right of the co-pilot/navigator seat was apparently a great place for a mouse to build a nest.

The cavity behind the panel to the right of the co-pilot/navigator seat was apparently a great place for a mouse to build a nest.

I left the nest alone for the moment and removed two screws from the block that went into the piece of wood I need to remove.  It appeared that a drain line for the front air-conditioner went through the floor near the outside edge and possibly some wires.  I left the nest for Linda to see and will resume working on this tomorrow.

Linda made vegan grilled cheese sandwiches for dinner and served them with some of the leftover broccoli soup and sliced fruit.  We each had a small glass of the Frey Natural Red organic/vegan wine.

After dinner I called Phil to see what his plans were for this week vis-a-vis our driveway and French drain projects.  I got his voice mail and left him a message.  When we left on Saturday afternoon he was just finishing up placing and compacting the gravel in the driveway but said the west end of the yard needed to dry out (again) before he could finish working down there.  Hopefully the new drain will help speed that process along.

The floor area under the driver’s seat in the bus with all of the rotten wood cut out.

The floor area under the driver’s seat in the bus with all of the rotten wood cut out.

Phil uses a self-leveling laser level system to measure elevations.  Not only has he assured me that the new 40 foot parking area is level, he has demonstrated it with his system.  Still, it does not look level, especially from certain points of view, and it does not feel level when driving in it, although that may also be an optical illusion.  We have a transit level and I plan to use it to check the pad, but it requires two people, one to hold the measuring stick and one to look through the telescope and record the readings.  That means I need Linda’s assistance, which means this will have to wait until the weekend.  Perhaps by then I will have the cockpit in the bus repaired.  It’s also possible that Phil will have returned and completed the job, I which case I may have him help me use the transit as a check on his laser system.

We watched our usual lineup of Tuesday evening TV shows while Linda checked in on her online word games and I worked on this post.