Tag Archives: sheet metal nibbler

2015/10/17 (S) First Snow

Last night we removed the dining table from the back of my car and put it on the bed in the bus.  We then removed the two rear seats and put them in the garage.  We wanted the back of the Honda Element empty when we got up this morning as we do not usually have time to spare in the morning before driving to South Lyon for breakfast with the South Lyon Area Amateur Radio Club.

It’s always good to see our fellow hams and today was no exception.  We arrived just before 8 AM and stayed for over an hour.  We left around 9:15 and drove to Chuck’s shop in Novi to get the box with the two remaining lower windshields for our bus.  Chuck was already there and helped us load the box into the car.  The box was sized to hold five windshields but only had two in it so it was light enough for us to move by hand.  I knew it would fit in my car as we had measured it on a previous visit and I had checked the dimensions against the car.  We set one end on the tailgate, lifted the other end, and slid it in.  We chatted for a while, and looked at a project Chuck is working in for new front window shades, before heading home.

Phil was not at our house when we got home but he had obviously been there.  All of the concrete, and many of the rocks and boulders, were gone from the driveway extension area so I presumed he had loaded them in his truck and hauled them away.

The Converted Coach Owners (CCO) Halloween Rally was going on this weekend and today was the main day for activities.  We had intended/hoped to go to the rally but the progress on our bus remodeling has slowed over the last couple of weeks for various reasons, all legitimate, and it was not in a condition to travel or be used.  It’s not that things are not getting done; they are, just not as fast as we would like or need them to.  Among other things I have not yet secured the refrigerator and pantry.  We thought about driving over in the car but it was over two hours one way and we needed to spend what time we had available working on the bus and could not justify being gone.  Thanksgiving does not look/feel that far away anymore.  It also seemed ill-advised to be gone while Phil is here digging up the yard.

My main bus focus for today was completing the installation of the built-in sofa.  We had already set the plywood seat board on a blanket on the bus kitchen floor so I had access to the inside of the base/storage box.  I did not need Linda’s assistance for a while so she worked on her counted cross-stitch project.  Before starting on the sofa, however, I took care of a few other minor things.

First I replaced the alkaline batteries in the TempMinder thermometers with Lithium ones.  I then reset the minimum and maximum temperatures for the two remote sensors.  Sensor #1 monitors the freezer and sensor #2 monitors the fresh food compartment of the bus refrigerator.  The directions for the TempMinder suggest using Lithium batteries if the remote sensors will be in cold environments.

Next I got a piece of scrap SurePly underlayment to see how it would fit in the rabbited wood trim on the lower outside wall of the hallway.  I inserted it fully into a corner and marked the edges with a pencil.  It is approximately 3/16″ thick and fit nicely without being too tight.  With a layer of veneer it should be just right.  When I removed it the depth of the rabbits appeared to be 5/16″ to 3/8″.  I think the underlayment will make a nice base for hardwood veneer.  I will cut the panels 1/2″ wider (22-1/2″) and 1/2″ longer (28″) than the 22″ X 27-1/2″ dimensions of the framed opening and allow them to “float” just like a frame and panel door.

My last mini-task was locating the 1/4″ walnut veneered plywood we removed from the old refrigerator and measuring it to see if we had pieces big enough to panel the damaged area on the wall by the co-pilot seat.  I was pleased to find that the remaining pieces are large enough for this application.

By now it was 12:30 PM and my phone reminded me that we had an RVillage Ambassadors webinar/meeting at 1 PM.  Linda heated up some Amy’s Vegetable Bean Soup and made hot lentil loaf sandwiches with ketchup.  Yum.  We got our first snow flurries of the 2015-16 winter season during lunch and they continued off and on through the afternoon.  We moved to Michigan in May 1976.  It snowed on October 15th that year and we had snow on the ground every day until early April 1977.  While that has not held up over the years as a “typical” southeast Michigan winter it was very different from what we grew up with in Missouri and formed our first and most lasting impression of our adopted state.

I retrieved the link for the Go To Meeting from the RVillage website and put it in my web browser.  1 PM came and went with no meeting.  The meeting notice said “Saturday, October 17 at 10 AM PST” but they had clarified that was actually 10 AM PDT, which is 1 PM EDT.  We decided that perhaps they really meant PST, which would be 2 PM our time.  We tried again an hour later, but no meeting ever commenced.

When I finally got to work in the bus on the sofa I removed six screws, three each from two angle brackets, and pulled the entire base assembly out from the wall, giving me complete access to the HVAC duct and wiring chase.  Much of the final installation of the sofa involved this duct.

Powered and manual sheet metal nibblers with the opening Bruce just cut in the OTR HVAC duct and the piece of sheet metal that was removed.

Powered and manual sheet metal nibblers with the opening Bruce just cut in the OTR HVAC duct and the piece of sheet metal that was removed.

The ends of the plywood seat rest on two boxes with open ends that also serve as plenums for air from the OTR HVAC system ducts.  I needed to cut out rectangular openings in the vertical face of the duct to allow air into the back end of these boxes.  I used a 1/2″ drill to create starter holes at the corners of the openings and then used a manual sheet metal nibbler and a drill-powered reciprocating nibbler, both of which I borrowed from Chuck a few weeks ago, to cut out the sheet metal.  The two tools work differently but they both worked well and I was glad I had both of them for this task.  The powered nibbler created a lot of small metal debris so I vacuumed the whole work area very thoroughly when I was done nibbling.

The right (forward) end of the duct also had an extra hole in it where I did not need or want one.  I removed an old sheet metal patch plate and cut a new one to cover the area I needed to close off.  I ended up having to pre-drill holes as I spun the heads off two of my cheap sheet metal screws.  I had a heck of a time getting the shafts out, but I got it done.  This was just one more example of why seemingly simple projects always take longer than they should.

Phil returned while I was working on the sofa and continued trenching in the French drain.  I stopped to chat with him briefly and Linda came out to let me know she was headed to the grocery store.  I then got back to my own tasks and let Phil get back to his.

The left support/plenum box with the circular register hole cut in the face plate.

The left support/plenum box with the circular register hole cut in the face plate.

The open fronts of the two plenum boxes are attached to the inside of the vertical front support, which is 3/4″ walnut veneered plywood.  To get the air out of the boxes and into the coach my design called for brown plastic 4″ round louvered diffusers.  They are considered “four inch” because the two inch long cylindrical pipe on the back will just fit through a 4″ diameter circular hole.  (A 4″ flexible duct, like dryer duct, will also just fit over the pipe.)  The visible part of the diffuser is actually 5-1/2″ in diameter.

The inside width of the plenum boxes is 4-1/4″ by design.  I needed to center a 4″ hole within that space so I had to locate the center point for my 4″ hole saw very accurately side-to-side.  I also wanted the hole centered vertically.  Using my small square I marked the vertical midpoint on the edge of the front plywood at each end.  I then measured in 2-13/16″ from the midpoint mark and used my spring-loaded center punch to mark the center of the hole.   [The 2-13/16″ dimension came from half the inside width, or 2-1/8″, plus the thickness of the plywood used to make the plenums, or 11/16″.]

A close up view of the nylon mesh screen material used to cover the opening in the HVAC duct to keep critters that might get into the duct from getting into the support/plenum box.

A close up view of the nylon mesh screen material used to cover the opening in the HVAC duct to keep critters that might get into the duct from getting into the support/plenum box.

I stood the boxes on their back ends so the front board was horizontal.  I straddled the front board with my legs to hold it and drilled starter holes with a #6 countersink bit.  I then drilled the 4″ holes with a 4″ hole saw using my 1/2″ Craftsman corded drill, being careful to have the pilot bit in the starter holes and drill perpendicular to the face of the plywood.  I have had this drill for 37 years.  It is very powerful and has several ways it can be gripped quite securely.  It is large, heavy, and lacks the convenience of a cordless drill but when I need to use a bit with a 1/2″ shaft and/or need the torque, this is still the drill for the job.  The hole saw created some sawdust so I vacuumed the whole area thoroughly when I was done drilling.

I was just finishing this work when Linda got back from the grocery store.  She put the groceries away and came out to see if I needed any assistance.  I already had the roll of plastic screen in the bus and she got the Gorilla Tape from the garage.  I cut pieces of the screen large enough to cover the two rectangular openings in the HVAC duct and used lengths of Gorilla Tape to secure them.  We then slid the base/storage assembly back into position, pushed it tight to the HVAC duct, and reattached it to the wood wire chase on top of the duct.  The two support boxes and the return air box have foam weather stripping on the back edges to seal against the duct.

We picked the plywood seat up off of the kitchen floor and set it back in place but did not secure it.  We left it out several inches from its original position and got a seat and back cushion from the bedroom.  We experimented with different spacings and finally agreed that we need to have the seat out 4-3/4″ farther than originally designed.  The current hinge board is 11/16″ plywood, 2-3/4″ wide by just under 78″ long.  This board is screwed to the top of the wiring chase and to one side of the 72″ piano hinge.  I will replace it with a piece that is 7-1/2″ wide by the same length.  I will also have to provide some additional support for the seat side of the piano hinge as in the original design had both sides of the hinge resting on top of the wiring chase on top of the HVAC duct.

The Tulip Tree behind our house in its full fall glory.  This is the first photo to be posted in this blog taken with the new Sony a99v DSLT camera.

The Tulip Tree behind our house in its full fall glory. This is the first photo to be posted in this blog taken with the new Sony a99v DSLT camera.

That was the end of the interior bus work for today.  By the time we were done Phil had driven his front-loader onto his flat-bed trailer and secured it so it appeared he was wrapping up for the day.  I chatted with him about the project for 30 minutes before he left.  Earlier in the afternoon I had found my site plan drawings for the bus barn and agreed to stake out the driveway tomorrow so we could review it first thing Monday morning.

Linda had invited Meghan and Chris for brunch tomorrow but it was not a good weekend for them as the Michigan vs Michigan State football game was taking place in Ann Arbor.  Chris manages the Pizza House restaurant, and being away on football Saturday is not an option.  They will come next Sunday (31st) instead.

For dinner Linda made a nice salad of mixed greens with dried cranberries, sliced almonds, and diced onions dressed with raspberry vinaigrette.  The main course was pan-fried polenta with vegan puttanesca sauce.  It held its heat to the last bite and was very satisfying on a cold evening.  I opened a bottle of Cupcake Black Forest red wine.  We have had it before and, although drier than I prefer, it went well with the meal.

After dinner I got my flashlight and checked the bus for axle/hub seal leaks by looking under the bus from the opposite side to see the inside of the wheels.  I did not see anything to suggest a problem on any of the six positions and will text that information to Joe tomorrow for planning purposes as he would require a second day to work on the seals if that was needed.

We spent the last couple of hours of the day in the living room, with the fireplace turned on, reading, writing, and playing games while enjoying some red grapes for dessert.  Linda got a text from her sister-in-law, Mary, with a photo of her and Ron “standing on ‘the’ corner in Winslow, Arizona.”  Ron has been retired for many years but Mary only recently retired and they are on their first extended camping trip in their A-liner trailer and their first trip to the southwest U.S.

We went to bed around 10 PM.  Linda fell asleep quickly while I divided my attention between cooking shows on the Detroit PBS Create channel, a concert by Eric Clapton on PBS, and working on this post.

 

2015/10/07 (W) The Root Cause

We had Linda’s homemade granola for breakfast with fresh blueberries.  Berry season is just about over for the year and they will become more expensive as they have to be transported from farther away.  I made a pot of Sweet Seattle Dreams, the half-caff blend that Jeff makes just for us, and we drank it in the living room.  Linda checked in on the world and pulled up the latest video from NutritionFacts.org while I researched hardwood veneers on Rockler.com.

After breakfast and coffee I called Metro Environmental Services to arrange to have the culvert under the road cleaned out.  They were able to schedule us for this afternoon so I accepted that appointment.  I then called Brighton Honda to check on my car and left a message for Rob, the service advisor who wrote up the repair for the driver side door lock.  I had no sooner left that message than I got a call from Karen at Bratcher Electric.

Mike had worked up the quote to install the 100 Amp disconnect, tie it into the output of the transfer switch, and run a 100 Amp 4-wire service entrance cable to the current sub-panel, making it into a main panel.  They would also disconnect and cap the current sub-panel feed from the basement as part of the work.  At just north of $1,300 it was a good $300 higher than I expected.  My expectation, however, was not based on anything specific other than my own sense of the cost of materials and the amount of labor that might be involved, plus a desire for it to not cost more than $1,000.  🙁

With the phone calls taken care of we worked in the bus for the rest of the morning.  Linda worked on stripping the remnants of wallpaper that remained after we removed the mirrors from the lower outside hallway wall yesterday.  I worked on re-routing the heater hoses for the fan-coil heat exchangers.  She got her job done before I got mine done.  That’s usually the way it is.

To start, I removed one of the old 4″ round plastic grates and used my inspection mirror and a flashlight to examine the inside of the HVAC duct.  What I discovered was that the two heater hoses were secured periodically with plastic cable clamps to the outer wall of the HVAC duct.  I also discovered that the metal part of the duct is just the inner wall and top.  The bottom is the plywood subfloor of the bus and the outer wall is the plywood wall.  As originally built the metal portion of the duct could be removed but when Royale Coach did the conversion they built cabinets around the ducts and put wood wiring chases on top of them in such a way that they can no longer be removed without partially disassembling the coach.

The location of the hoses and wires in the duct was such that I could safely use my 4″ bi-metal hole saw to cut access holes for the hoses.  I determined where the cable clamps were located by measuring inside the duct.  I then marked where the access slots in the bottom back of the bases would be located and determined where I needed the two hoses to emerge from the duct.

The manual sheet metal nibbler used to cut a line between the bottoms of the two holes in the HVAC duct.

The manual sheet metal nibbler used to cut a line between the bottoms of the two holes in the HVAC duct.

There was already a 4″ hole at one of my needed locations so I drilled a second one next to it with an inch in-between.  I used Chuck’s hand powered sheet metal nibbler to connect the holes together to make an opening that looked like the track around a football field.  We vacuumed up the metal chips and I then installed door edge molding all the way around the edge of the opening.  I was able to reach the screws holding the first pair of cable clamps with a #2SR screwdriver and remove them.  This large slot will be behind the left end of the center connecting cover of the desk and the hose for the heat exchanger that goes in the left base will come out of it.

 

Plastic U-channel door edge molding installed around the new heater hose opening.

Plastic U-channel door edge molding installed around the new heater hose opening.

The location of the next pair of cable clamps corresponded, roughly, to where I needed the hose for the right heat exchanger to emerge.  I drilled two 4″ holes, side-by-side, at that location and nibbled out the little bit of metal in-between them to make a second slot.  Again, I installed the door edge molding around the entire edge.  The molding was a tight fit, and I had to use a screwdriver to get it to go on the inner curves, but I got it on.  The U-channel is locked in mechanically and has adhesive in it so it should stay put once it has had a few days in place.  Once the hoses are re-routed I will put screen material, and perhaps some solid plates, over the openings to prevent critters from gaining access to the living area by way of the HVAC PCTS (Prevost Critter Tunnel System).

 

The access holes in the OTR HVAC duct in the area behind where the desk will be installed.

The access holes in the OTR HVAC duct in the area behind where the desk will be installed.

Linda had two medical appointments this afternoon, both routine diagnostic procedures, so she got cleaned up, changed her clothes, and left around 12:30 PM as I was finishing up the second slot.  I went inside and was thinking about making something for lunch when the doorbell rang.  It was our mail carrier, Michelle, with a package that was too big for the mailbox.  A few minutes later the doorbell rang again.  I figured it was Michelle again, but it was one of the guys from Metro Environmental Services.  They were supposed to call first but just showed up.

I put my shoes on and walked them down to the clogged culvert that goes under the road.  I was really hoping they could clean it out from the south side but when we went into the woods we could not see the end of the culvert.  They got a metal detector and located the end of the pipe.  It was almost completely buried and had a massive root running right in front of it from a very large nearby tree.  They got a shovel and dug out around the root, exposing much of it and the end of the pipe.

The tree was probably 30″ in diameter at the base and the root was at least 10″ in diameter.  I got my (new) 18″ chain saw but had trouble getting it started.  It turned out it was out of gasoline.  Once I got it started I tried to cut through the root on either side of the culvert.  I thought I was all the way through on one end (closest to the tree) and most of the way through on the other end, but the root would not budge.  I dulled the teeth on the chain to the point where the saw would no longer cut and did not want to take the time to put a new chain on just to ruin it quickly.  The guys finally agreed to hydrojet the culvert from the north side of the road.

The actual cleaning out of the culvert did not take that long.  The pump produces 2,000 PSI and they used about 300 gallons of water from the onboard tank on their truck.  The head on the end of the hose has one forward facing nozzle and many rear/side facing nozzles.  The forward facing nozzle loosens and cleans out the area directly in front of the head while the other nozzles force the head forward and blast whatever is in the pipe back out towards the entrance.

They started with a small head and ran it in until there was water coming out the other end of the culvert.  They then pulled the hose back and switched to a much larger head and ran that all the way through and back.  When they were done muddy water filled the culvert and the depressions on either end.  On the inlet end the water was only about 3″ deep in the bottom of the culvert but on the outlet end it was near the top.  They billed me for the minimum first hour amount even though I think they were here longer than that.

I called Phil to let him know what we had run into.  He was surprised, to say the least, as he thought he had checked the other end of the culvert.  Obviously not, but that’s water under the road, so to speak.  Besides the problems with the root and the discharge end of the culvert being below the surface, it looked to me like the discharge area was something of a low spot and it was not obvious to me where water would flow from there.  I have learned, however, that I am not very good at judging such things visually.

Cory, our neighbor across the street, had come over to see what was going on.  He offered that the discharge area does, in fact, drain to the south through his property and eventually to Golf Club Road.  Cory has been here for 30 years so I have no reason to doubt the truth of that.  The elevation where Golf Club ends at Hacker and where our street ends at Hacker appears to be about the same.  Our street is fairly level while Golf Club has a little bit of up and down, but it is subtle.  I suggested to Phil that we might have to clear a path into the woods for his small digger and do some trenching to give the water a way out.

While Cory and I were chatting I noticed that the trees along this part of the road were hanging out over the road on both sides and were rather lower than they should be.  This is the very thing I complain about with regards to the way most of our neighbor’s fail to maintain their properties along the road.  I decided I should do something about it so I got our pole saw and spent a couple of hours trimming the low overhanging branches.

Linda went to the Whole Foods Market in West Bloomfield following her medical appointments and got home just as I was finishing up the pruning.  She went for a walk while I called John Palmer of Palmer Energy Systems in Florida.  I bought our Magnum inverter/charger for the bus from John along with various accessories and batteries.  I needed a 4-wire terminal block for our Magnum Battery Monitor Kit (BMK) because I had messed up the one that came with it when I originally installed it.  John confirmed that Magnum Energy had recently been acquired by Sensata, and was in the process of relocating the plant to Minnesota, but that several of the old-timers were still on board.  John needed to talk to Tom anyway and asked me to call him back in a week to see if he was able to get the connector.

I checked with the service department at Brighton Honda again and Rob said he expected to get the new door lock mechanism back from the locksmith tomorrow morning and to have the car ready for me to pick up by the end of the day.  It will be nice to finally have it back.

The cloudy weather finally broke today and we saw some blue sky with brighter light levels than we have had recently.  The day was lovely but a little on the cool side by late afternoon so we both had a cup of hot tea.  Linda took advantage of the light to work on her counted cross-stitch project, a holiday stocking for grand-daughter Madeline, and I went back to the bus to sand off the last traces of the old wallpaper from the outside wall in the hallway.

I used our Porter-Cable 1/4 sheet palm sander with 80, 120, and finally 220 grit sandpaper.  The sander has an integral dust collection bag but it does not capture all of the dust.  I used the vacuum cleaner to pick up as much of the residual dust as I could and then used a tack cloth to wipe down the wall.

For dinner Linda made pan-grilled tofu with caramelized onions in sweet barbecue sauce.  She served it open-faced on rye bread, because that is what we had, and steamed some fresh green beans as a side dish.  Yum.

After dinner I drove to Lowe’s.  I needed something I could use to plug the two heater hoses to keep them from leaking as I pull them back through the HVAC duct and out through the new slots I made for them today.  I ended up buying two 3/4″ barbed plastic plugs.  While I was there I looked to see if they had any bleeder valves but they did not.  They do not sell parts designed specifically for hydronic heating systems and I will have to go to Northwest Plumbing and Supply for such items.

While I was in the plumbing isle I looked to see if I could figure out some combination of parts to make a fill valve for the system but did not see anything that inspired me.  I would love to have one or more high point expansion tanks on this system but I do not have any easily accessible places for them from which I could also run overflow drain lines.  There is a good sized volume of unused space behind the drawers on the passenger side of the bedroom but it would be a very difficult place to install anything.  Perhaps Northwest Plumbing and Supply will have something.

On the way home I stopped at the BP station and topped up the fuel tank in Linda’s car.  I drove home with greater consideration for fuel economy than usual and managed to get the average MPG up to 56.7 before it dropped back to 55.4 as I pulled in the driveway.  It will drop into the upper 40s as soon as Linda starts the engine tomorrow morning but it was fun to get it into the driveway with numbers above 55 MPG.

 

2015/10/02 (F) Tire Nibblers

It dropped into the mid-40s last night and the house cooled off proportionally.  It starts getting light at 7 AM these days and cool mornings are just another reason to stay under the covers a little longer.  I finally got up at 7:30 AM, got dressed to work, and made our morning coffee.  After our breakfast of fresh mixed berries and homemade granola I turned on the fireplace and we enjoyed our coffee to its dancing light and warmth.

Chuck called to let me know he had set out one of his sheet metal nibblers for me to pick up at the shop.  I left around 10:30 AM and drove Linda’s Honda Civic to Discount Tire in Howell.  (My Honda Element is tied up at Brighton Honda until the middle of next week to get a broken driver-side door lock replaced.)  I noticed last night while we were out that several tires on the Civic were under-inflated and the sidewalls were badly weather-checked.  They still had plenty of tread but the paperwork indicated they were put on five years and 80,000 miles ago.  Time for a change.

At Discount Tire the sales associate confirmed that the date code was from 2009 and corroborated my observations.  The tread was probably good for another 20,000 miles but I do not mess around with old tires with cracked sidewalls.  Michelin no longer makes the Defender, at least not in the P195/65R15 size, so I bought a set of four Continentals that should perform equally well and last for 90,000 miles.  That means they will age out before the wear out, which is fine with me.  It was going to be a two hour turnaround time so I texted Linda and Chuck and settled in to wait.  Thank goodness for iPad games.

The technician pulled the car in at noon and a few minutes later asked me if I had the key for the wheel locks.  I had looked for it earlier and not found it.  He wasn’t sure he could get them off at all and would certainly ruin them in the attempt.  That sounded like a bad situation getting worse so I had them set the tires aside while I took the car to Brighton Honda and had them remove the special lug nut from each wheel using their master key set.  I bought a new set at the Honda dealership (so any Honda dealer can remove them in the future) and had them put those on and made sure I had the key when I left.

While I was there Rob gave me a quote on four Continental tires.  The installed price, including a rebate in the form of a Visa gift card, was 30% lower than the price I paid at Discount Tire so I showed the quote to the guy at the counter when I got back.  He said the quote was for a different, less expensive, discontinued tire.  I had no way of knowing if that was true or not but he also asked if the guy who wrote me up gave me the rebate form for the tires I bought.  I said ‘no’ so this guy printed out an extra receipt and gave it to me with the rebate form.  That narrowed the price difference to 20% and I was satisfied with that.  I liked the tires I had purchased and did not want to undo and then redo the sale.  I have also had good experiences over the years with Discount Tire, including their nationwide free rotation and balancing policy.

When the tires were finally mounted, balanced, and installed I headed for Chuck’s shop in Novi.  He was there when I arrived and had three different metal cutting tools laid out to show me.  One was manual, one was electric, and one was powered by a drill.  We decided that the manual one and the drill powered one were most likely to work for what I needed to do.  He put them in a cardboard box along with cans of three different chemicals he was getting rid of.  His trash, my treasurers.

On the way back to the house I stopped at the Shell station at Beck and Grand River Avenue to top up the fuel tank.  I texted Linda and then headed for home.  I arrived home at 3 PM to find lunch on the table.  That was a nice surprise.

After lunch we uninstalled the desk in the bus and set the pedestals on part of a large blanket in the center of the kitchen floor.  We draped the blanket over them and then uninstalled the hinged sofa seat and set it across the pedestals.  We folded the blanket back over the seat and set the desk bases on top of it.  We now had clear access to the wall behind the desk and the wall behind the sofa.

I got a 3″ brush from the basement and then got the Zinzer 123 Primer, opened it, and stirred it.  It was still in good shape as it has been in the library since last fall when we repaired and repainted the west wall after Darryl was done installing the new HVAC system.  Rather than pour it into another container I found a lid from a copy paper box to put it under the one gallon can.  Linda finished masking off the woodwork and counters in the bus and then helped me spread painter’s plastic to protect the floor.  We spread out an old bathroom towel, put the box lid on that, and then put the can inside the (upside down) box lid.  I set the can lid aside and worked directly out of the can.

I started in the back of the hallway and primed the upper half of the outside wall as I worked towards the front.  The lower half of this wall has vertical mirror tile wainscoting.  We wanted to remove it but assumed the pieces were glued directly to the plywood wall, as they are elsewhere in the coach, in which case removing them would have done a lot of damage.  We repositioned the plastic, towel, and paint and I continued up the passenger side priming the plywood next to and (mostly) under the windows.  Completing that side up to the cockpit required one more repositioning of all the stuff.  I was working in close proximity to the new living room captain’s chairs so we wrapped those in painter’s plastic as well.

Bruce primes the bare plywood behind the sofa and under the driver side living room window.

Bruce primes the bare plywood behind the sofa and under the driver side living room window.

I moved to the driver’s side and primed the area under the window and up the left side.  Even though Linda had masked off all of the woodwork with painter’s tape I worked carefully and stayed away from the tape.  We are not sure that the priming is even necessary and I did not want to risk getting any on the woodwork.

By the time we finished it was 5:30 PM and we were done working on the bus for the day.  We had only worked for a couple of hours, and only accomplished a small task, but it was a critical path task that stood in the way of getting a whole chain of other important things done.  Tomorrow we will sand the primer with 220 grit paper using the palm sander and try hanging the new wallpaper.

Linda made a pizza for dinner using the gluten-free almond meal recipe she got from Mara.  She topped it with greens, onions, mushrooms, sun-dried tomatoes, and Daiya non-dairy cheese.  There is also cheese in the crust along with garlic and other good things.  We had a nice salad first with walnuts, beets, and sun-dried tomato vinaigrette.  The salad was very good and the pizza was outstanding.

Philip Jarrell called to let us know he would be here at 8 AM tomorrow to start our French drain and driveway project, weather permitting.  Detroit Public Television shows classic movies at 8 PM on Fridays and tonight’s selection was “Bullit” starring Steve McQueen and Jacqueline Bisset.  We watched This Old House and a couple of travel shows after that and then went to sleep.