Tag Archives: Blue Ox tow bar

2015/09/14 (M) Final Prep (for now)

We were up at 8 AM and had breakfast but I did not take the time to make coffee.  I gathered up the laundry and started a load.  I then headed to Lowe’s to buy an outlet strip that I could easily hardwire.  I looked at angle iron to support the upper back edge of the interpedestal desk cover at the wall but did not buy any.  The iron has holes and slots manufactured into it that I thought might allow me to adjust its location vertically without having to move the location of the screws.  Alas, the slotted openings were horizontal rather than vertical.

Linda was cooking a batch of granola when I got home and made a pot of coffee.  I decided to tend to some travel preparation items before getting back to work on the remodeling project.  I wanted to check/adjust the tire pressures while it was still cool.  The tires were all down about 1.5 PSI, which was very good given how long it has been sitting.  I used the new 6-gallon air-compressor to bring them up to the pressures I like to run and it worked OK.  I will have to pause a little more often while it re-pressurizes but it is less than half the size of the 15-gallon DeWalt and will travel with much more easily.

My next task was to unload the front bay which I did while Linda continued to work on our food for the week.  We find it much easier to deal with food at rallies if she “cooks ahead” and “reheats to serve.”  I set everything in the driveway in front of the bus and tried to sort it into two groups; things were staying home for this trip and things that were going with us.

I then opened the drain valve on the fresh water tank, which goes through the floor of the water bay, and let the water run onto a container lid so it wouldn’t dig a hole in the gravel driveway.  I was getting ready to deploy the fresh water hose(s) when I noticed that they were in need of some serious cleaning.  Linda agreed to take care of that and cleaned their storage tub too.  Ditto for the waste water (sewage) hoses and their storage tub.  Her taking on this task allowed me to return to working on the installation of the desk.

I had a 12″ long piece of 1/8″ aluminum angle and decided to use it to support the upper back edge of the interpedestal shelf/cover.  I drilled and countersunk five holes in one of the flanges.  Linda finished cleaning the hoses and then got our wireless thermometer from the house.  It has a base thermometer and two wireless remotes so she put one remote in the freezer and the other one in the fresh food compartment.  We wanted to monitor the temperature and dial it in to where we needed it before loading the refrigerator with food.

The stacked mending plates used to create a tongue-&-groove alignment system between the center cover and both the left and right desk pedestals/bases.

The stacked mending plates used to create a tongue-&-groove alignment system between the center cover and both the left and right desk pedestals/bases.

I removed the interpedestal cover and set the left pedestal aside so I could complete the AC wiring connections.  I mounted the outlet strip to the wall centered between the two pedestals and about two inches below the level of the underside of the plywood that will support the Corian top.  The outlet strip had a 15 foot cord.  I determined how much of that length I needed to get through the right pedestal and forward along the wiring chase to where the other wires were located.  I cut off the extra length, routed the power cord into the right pedestal at the left upper rear corner, down the inside left rear corner, and out the left end of the upper base.  From there it ran forward to the other wires where I connected them.  I turned on the circuit breaker and then turned on the outlet strip.  The switch lit up, indicating the presence of 120V AC.  I used my Etcon tester to check the duplex outlet by the passenger seat.  It also had power so the wiring was good.

I set the interpedestal shelf/cover back in place, aligned with the right base, and then aligned the left base to it.  I checked the distance from each end of the base to the HVAC duct and adjusted it to be the same.  We then adjusted the position of the left pedestal until we were satisfied with the alignment with the interpedestal cover.  We checked the alignment of the front top edges of the pedestals with a 6′ metal ruler.  Everything looked OK so I secured the pedestal to the base using two screws that will be hidden by the laser printer in normal use.

I needed to screw the pedestal to the wall in the two upper corners to minimize the visibility of those screws.  It was not flush to the wall at those points so I used a shim in the upper right.  We will have to cover the vertical gap at the left rear with molding.

Bruce finds the center of a drawer front by finding the point where the diagonals of the face intersect.  The handle mounting holes were located horizontally 1-1/2” to either side of this center point.

Bruce finds the center of a drawer front by finding the point where the diagonals of the face intersect. The handle mounting holes were located horizontally 1-1/2” to either side of this center point.

We put the removable plates back in the bottom of each pedestal.  I drilled the holes for the pulls in the four desk drawers, installed the pulls, and put the drawers back in the desk.  To find the correct location for the holes Linda suggested that we put a piece of painter’s tape in the center of the face and then draw a small segment of the two diagonals to find their intersection.  For the two small drawers that was all we needed as they got single knob style pulls.  For the two larger drawers we needed to locate the holes 1-1/2″ to either side of the center on a line through the center parallel to the top and bottom edges.  I measured carefully and I think we did a pretty good job.

Sometime during the morning I texted Jarel the dimensions for a 3/4″ thick piece of walnut 1-7/8″ high by 34″ long to use as a face for the edges of the three layers of plywood under the refrigerator.  He texted back and said “no problem” which lead to an exchange of a dozen e-mails clarifying just exactly what I wanted.  I did not mind, better that than assumptions that result in wasted time making parts that don’t fit.  Jarel is an experienced cabinet maker and is meticulous in his work.  He knows all the questions to ask about things I did not specify and does so before cutting any wood.

Our last construction task before departure tomorrow was rehanging the bathroom door.  I measured the distance from the bottom hinge to the bottom edge of the door and compared it to the distance from the hinge in the door frame to the floor.  It looked like it should fit without rubbing so we hung the door.  (The old ceramic tile rubbed as the door was swung to its fully open position, but the thickness of the underlayment and vinyl tile is less than the ceramic and thinset, at least in that area.)

Linda was still trying to prepare our food for the rally as there will be very little of the included food that we can eat.  She made a grocery run while I returned to emptying out the front bay of the bus.  I plan to leave most of the stuff that was stored in that bay at home so Josh has access to the ceiling to see if we can through-bolt mount the two captain’s chairs in the living room.  I might also store all of the GLCC stuff down there as Linda will be coming down on Wednesday in the car with the cats and we want to minimize the amount of other stuff in the car.

I thought about sanitizing the fresh water system by using the 12V DC water pump and the winterizing valves/tubes to draw a dilute chlorine solution from a bucket and pump it through the fresh water pipes.  I decided against it based on available time and higher priority items that needed to be done.  I connected the clean fresh water hoses to the coach and started filling the tank.  I checked that the fuel polishing pump was off and checked the air springs and latch on the generator.  I made a mental note that the aft air springs (front of the Yanmar diesel engine) needed air and made sure the slide tray was latched in place.  I was going to start the generator and let it power the air conditioners but decided to forego for now that as well.

We had unlatched and removed the towbar from the bus receiver earlier in the summer.  I used one of our hand trucks to move it over by the car.  I put the passenger side rear seat down and loaded the towbar in behind it along with the bag that holds all of the other pieces.  That left plenty of room for the two cat carriers, litter tray, and any miscellaneous things she may bring along on Wednesday.

We put the mattress back onboard and Linda made the bed, but forgot the electric heating pad.  Linda did some cleaning and then we loaded clothing and food.  Computers, cameras, and other technology will go on first thing tomorrow morning.  We then got the various GLCC items out of the garage and staged them by the passenger side of the bus.  I loaded our personal items onto the driver’s side half of the slide tray and loaded the GLCC stuff onto passenger side half.

Our goal was to be done by 5 PM but it was 6 PM when I finally had the pressure washer ready to use.  It took me a little over an hour to spray the car and the coach and I wrapped up for the day at 7:30 PM.  We had seitan stroganoff for dinner with the 2013 Egri Merlot and had watermelon for dessert.  It was another long day but we got a lot accomplished and most it did not require me to work on my hands and knees, for which I was grateful.

 

2015/05/16 (S) Trucks and Buses

To paraphrase, “If it’s Saturday we must be in South Lyon” and that was, indeed, the case.  Most of the regulars were missing from our weekly breakfast gathering of the South Lyon Area Amateur Radio Club (SLAARC), but six of us showed up and had a great conversation.  By the time we headed towards home it was starting to rain lightly.

We stopped at Brighton Honda to get some information on the Honda Ridgeline pickup truck.  The salesman was very nice, but unfortunately Honda has stopped making the Ridgeline.  They are reintroducing it in the fall of 2016, but we will likely make a decision about a new car/truck sooner than that.  There are still a few in stock around the country but we already have an orphaned Honda Element.  We like the car, but would be happier if they were still being made.  In this case, however, it was a moot point as the Ridgeline is not towable four wheels down.

We drove next door to Brighton Ford to look at F-150 pickup trucks.  We were assisted by Frank Stapleton and he was easy to work with.  He insisted that we meet his new car sales manager, Eric Wilkinson, before we left.  We felt that was unnecessary at this stage in the process, but he also seemed like a nice enough guy.  The entry level XL 2-door may be reasonably priced (not really, but what car is?), but the slightly nicer XLT 4-door short bed with 4-wheel drive, towing package, and off-road package looks like it would price out at $45,000 give or take three grand.  Without X -Plan pricing that is simply not going to happen, and even with X-Plan pricing it is not a sure thing.  Frank really wanted us to test drive one but given the rainy weather we were not in the humor to do that today.

The F-150 is a nice truck, nicer in fact than many cars, and perhaps nicer than a pickup truck needs to be or should be.  On the plus side it certainly has ground clearance, but on the negative side (for us) it is also BIG.  The back seat room in the four door body style is cavernous, made larger by fold up seats, and that would be very useful for us when traveling in the bus.  Between the back seat and the bed we could store a LOT of stuff.  It has well-placed handles by all four doors, and it is a god thing as we both needed them, along with the running boards, to get in and out.  There are several engine options including the 2.7 L and 3.5 L Eco-Boost models, both of which feature twin turbochargers.  These are high-tech engines, with incredible power and torque and decent fuel economy. I liked the sound of that, but unfortunately that technology comes at a significant price premium.  Interestingly, Ford is using an aluminum body and the truck weighs in at about 4,700 pounds.  Our Honda Element weighs over 4,000 pounds and it is not nearly as big as the F-150.  How well the aluminum will hold up is unknown.

We were almost home when we decided to keep driving and visit LaFontaine Nissan.  While not as convenient as the Brighton dealerships, it is only 15 miles from our house, 13 of those headed east on M-59.  Linda checked their hours on her phone and they were open until 4 PM.  The purpose of our visit was to look at the Nissan Frontier pickup truck and the Nissan Xterra SUV, both of which Edmonds.com suggested were viable off-road alternatives to a Jeep Wrangler while Consumer Reports indicated they were more reliable and more practical than a Jeep Wrangler.  Bobby Lundwall, the Commercial Manager, assisted us and we met the General Sales Manager, Don Poley, before we left.  Bobby was very helpful and brought a Frontier and Xterra around front for us to see.  Again, we were not interested in test driving one at this stage, especially in the rain.

The Nissan Frontier pickup has an available 4-door, 4-wheel drive, short bed model.  It is considered a mid-size truck and is noticeably smaller than a Ford F-150 in every way.  The Pro-4X off-road version has 10.1 inches of ground clearance at the differential, which should be adequate for our needs.  It has a transfer case but is only towable four wheels down with the 6-speed manual transmission.  We looked at the Xterra but found it harder to get in and out of, especially the back seat.  It is taller than the Frontier and after due consideration we agreed that we were not really in the market for an SUV.

The Frontier does not have the bewildering array of options that the F-150 has and would be more suitable for the 95% of our driving that is on local paved and dirt roads.  It would be perfectly adequate for hauling materials from Lowe’s to the house and has an available tent option for camping.  We presume that aftermarket bed covers, canopies, and even small truck campers are available but we would check on that before buying one.  Ditto for Blue Ox base plates and the ability to install an SMI Air Force One auxiliary braking system.

We did not test drive one, but it was easy to get in and out of, and comfortable to sit in, at least in the front seats.  It weighs about 4,500 pounds, basically that same as the much larger F-150.  The only negatives at this point are the manual transmission and lack of choice on interior fabric; the Pro-4X only comes with a charcoal interior, either cloth or leather.  The bottom line was that it is probably a better fit for us than a Jeep Wrangler or a Ford F-150 and could be acquired for under $35,000 equipped the way we want it.  Nissan also has zero percent financing available at the monument, although that is often in place of other incentives.  The fact that it requires a manual transmission to be towed four wheels down, however, probably knocks it out of contention.

Storage compartment under the lift-up bed platform.  The two boxes concealed and protectd 4" flexible HVAC ducts.

Storage compartment under the lift-up bed platform. The two boxes concealed and protectd 4″ flexible HVAC ducts.

Once we got home we had a light lunch.  I then changed into my work clothes and got back to work deconstructing the inside of our motorcoach.  (I like the term deconstructing as I think it is more descriptive of what I am doing that demolishing or even disassembling.)  My goal for today was to finish removing all of the carpet and all of the carpet tack strips.  I accomplished all of that except for a piece of carpet on the wall behind the driver’s seat and a piece on the front wall of the entry stairwell.  My first task, however, was to cut a short slot in the 3/8″ plywood filler that was under the dinette in order to free an AC electrical cable that ran through it and then through the floor.

Getting the carpet off of the sides of the bed platform was interesting.  There was a piece of wood trim installed along the top edge of the side of the bed base facing the front of the bus and just under the plywood bed platform.  The trim strip is rabbited on the underside and conceals a 12VDC strip light that is tied in with toekick lights in the bathroom and the floor lights in the hallway.  The power for the lights comes from inside the bed base through a small hole in the plywood and carpet.  The trim strip also appeared to be installed over the carpet and needed to be removed to get the carpet loose along the top.

Under-bed storage compartment with bot HVAC ducts uncovered.

Under-bed storage compartment with bot HVAC ducts uncovered.

There was also an adjustable HVAC louver on each side of the bed.  The louvers were installed from the outside and had flexible heater ducts slipped over them on the inside and secured with screws.  The flexible ducts were in the storage area under the bed and were covered by wood boxes to protect them.  The boxes, in turn, were carpeted to match the rest of the storage compartment.  To disconnect the wiring for the strip light and remove the boxes I had to first empty out all of the stuff stored under the bed so I could get in there to work.  The bed platform is hinged about one foot from the head end and the foot end lifts up, supported by two gas struts, so there was plenty of room to work once I emptied it out.

I have disassembled enough of the bus at this point to have some idea of how the conversion was built.  The cover “boxes” for the flexible ducts were actually half-boxes with a long side and top and one small end.  They were installed into a corner using a cleat screwed to the floor that the bottom edge of the long side was then screwed into.  There was a similar arrangement to catch the free edge of the top and it was screwed to the inside wall of the platform base.  All of these screws were put in through the carpet that covered the boxes and were essentially invisible so I had to find the screw heads by touch and back them out.

The area just forward of the bed base with the bed platform raised and facing the driver side of the bus.

The area just forward of the bed base with the bed platform raised and facing the driver side of the bus.

Once I got the protective boxes loose I discovered that the floor and wall were also carpeted.  There was a small bump out in each rear corner that served as wiring chases for AC electrical outlets on each side of the bed, and these bump outs were carpeted.  It seemed clear to me that the HVAC ducts, which are part of the OTR HVAC system, may have originally been installed directly into the HVAC chase outside the bed base and later repositioned to the sides of the bed thus requiring the louvers, flexible ducts, and cover boxes.  They also greatly reduced the available storage space under the bed.

The OTR HVAC chase runs along the floor-wall junctions on both sides of the bus for most of the length of the coach and a 12″ section of it is accessible on either side of the bed.  Removing the two flexible ducts, sealing up the openings, and installing the louvers outside the bed platform will free up additional storage space under the bed which is a good thing as we can always use for storage space.  That’s a nice bonus but adds some additional work to the remodeling project.  Such is the nature of remodeling; you never really know what you have until you have completed the deconstruction phase.

The aft side of the bed base.  There is not a lot of room to work in here so I will remove the bed platform when I install the new tile floor.  I plan to use the same tile on the sides of the bed base.

The aft side of the bed base. There is not a lot of room to work in here so I will remove the bed platform when I install the new tile floor. I plan to use the same tile on the sides of the bed base.

It was overcast all day with humidity near 100% and rained off and on into the evening.  It was also warm so I kept opening the roof vents and running the fans to make it more comfortable in the coach, but every time I did it started raining shortly thereafter.  When I was done working on the bus for the day I moved the ten concrete blocks that had been supporting the propane tank for the whole house generator and pulled up the utility marker flags for the underground gas line to our meter.  Keith will be here to cut the grass this coming week and I want him to be able mow these areas.

Linda spent the afternoon thoroughly cleaning the kitchen.  She also prepared a sugar-water solution, filled the hummingbird feeder we bought at Lowe’s the other day, and hung it off the railing of our rear deck.  A hummingbird found it almost immediately which was very cool.  For dinner Linda made pan-grilled tofu slices with caramelized onions and sweet BBQ sauce served on tortillas.  She also sautéed fresh broccoli and sliced up some fresh strawberries and pineapple.

After dinner Linda went to the Edmonds.com website to see if she could get a better feel for dealer cost and Fair Market Value for the Ford F-150 and Nissan Frontier.  While she was at it she looked up the Chevy Colorado (GMC Canyon), and Toyota Tacoma.  The Chevy Colorado was Motor Trend Magazine’s 2015 Truck of the Year.  Both the Colorad0/Canyon and Tacoma are mid-sized pickup trucks.  Toyota’s full-size pickup is the Tundra.

Brendan called while we out to see if Linda could sit with Madeline tomorrow night while he and Shawna had dinner with their friend Jorge.  Depending how the day goes tomorrow I may go to Ann Arbor with her.  We had two episodes of Sherlock left to watch and the DVDs have to go back to the library on Monday, so we watched both of them this evening.  It was a double feature so I made popcorn in-between episodes.

 

2014/10/16-22 More Bus Work

2014/10/16 (R) More Wiring

Butch had to go to Logansport this morning for parts and groceries.  I stayed behind to continue working on the AC wiring for their bus conversion; after breakfast, of course.

I mounted two 6-position AC main lug panels, one above the other, to the right of the 20-position panel we installed yesterday for the inverter circuits.  The panels I installed today were for AC circuits that only run on shore power or the generator, not the inverter.  The reason for two panels was: A) Butch already had them, and B) they were narrower than the larger panels and would fit in the available space on the right rear wall of the closet.

I had tied the main shore/generator power line to the inverter AC input line last night so the refrigerator, which is wired through the inverter panel, would have power overnight.  I left those tied together for most of the day so the lights would work.  I pulled all of the existing circuits that we disconnected yesterday into the boxes, dressed the wires, and connected/mounted the circuit breakers.  By the time I finished Butch had returned from his morning errands.  He connected the shoreline and I checked to see that we had 240 VAC between L1 and L2 and 120 VAC from each line to the neutral conductor.  He then disconnected the shoreline and made sure the generator was off.  Using the inverter to power a work light, I pulled the main power cable into the lower box and secured it.  I then pulled the cable that feeds AC power to the inverter into the lower box and connected it to a 30 Amp breaker.

MC-9 house wiring.  Inverter panel on the left, shore/genset panels on the right.  DC upper left, solar upper right.

MC-9 house wiring. Inverter panel on the left, shore/genset panels on the right. DC upper left, solar upper right.

I plugged the shoreline back in but got a low voltage with no current on L2 and an Error Code 6 on the Progressive Industries EMS remote monitor display.  Butch checked the plug and I just did not have it fully inserted into the outlet.  Once he fixed that we got the correct voltages and no errors.  We checked each circuit and everything checked out perfectly.

(Note: The shoreline is wired for “50 A” RV service, which is 240 VAC service from L1 to L2 but with an active neutral that provides two 50 A, 120 VAC power feeds with L1 and L2 180 degrees out of phase.  As a result the currents in the neutral wire from L1 and L2 cancel rather than add.  Butch has his generator wired for 120 VAC output and has L1 and L2 tied together on the generator side of the transfer switch.  This makes the full 100 A output of the generator available to be shared between L1 and L2 in any proportion.  Although this system can supply a full 50 A of current on both L1 and L2 at the same time, it could also supply 70 A or one and 30 A on the other unless this is prevented by circuit breakers.  Also, regardless of the distribution of current between L1 and L2 the currents will add in the neutral as much as 100 A of current.  Although sensible load management would prevent this from ever happening it is entirely possible to draw 30 or 35 A on each leg and end up with 60 – 70 A in the neutral.  Thus, when designing your house AC electrical system this way, provision should be made for a neutral conductor that is sufficient to carry this amount of current.  The advantage to doing your system this way is that the voltage regulation will be better under load than with a 240 VAC generator powering imbalanced 120 VAC loads on both legs as the 240 VAC configuration regulates the voltage between L1 and L2 but the voltage from L1 to N and L2 to N can be off substantially.)

Butch needed another non-inverter circuit for the front of the bus so we pulled a 10-2+g Romex cable from the electrical closet along the driver’s side wall/ceiling area and down into the cabinet at the front end of the kitchen counter. He and Fonda spent a bit of time cutting openings in the end of the cabinet for a two-gang outlet box and a single-gang outlet box.  The two-gang box was for a pair of duplex outlets fed from the inverter panel and the wires were already run.  The single-gang was for the new circuit we just pulled.  When they were done I disconnected the shoreline so I could safely tie the new circuit into the lower panel.  I then installed the cover plates on all three boxes and plugged the shoreline back in.  We had the breaker turned off for the new circuit while I wired the outlet.  I then energized it and it tested OK.

I repositioned a 12 VDC fused distribution box above the inverter panel and mounted it.  I then moved a terminal strip for their solar panel wiring to a slightly different location to open up a space for Butch to drill a hole.  At that point we were done working for the day.  I changed into my non-work blue jeans and relaxed for an hour before dinner.  During that time Butch called Jaral Beatty, a cabinet maker in Logansport and personal friend of Butch’s, and put me on the phone with him to see if he could come to Twelve Mile and finalize plans for a custom desk and printer cabinet for the bus.  The weather forecast for tomorrow is for mild, mainly sunny, conditions and Jaral said he could come out mid-afternoon.

Butch and Fonda’s younger daughter, Brittani, and her husband, Sterling (Rock), were expected for dinner at 7:00 PM so I fixed a salad and heated some Amy’s chili for my dinner.  Dinner was jovial and the first time I have eaten with Butch and Fonda at home on this latest round of working visits.  Butch called Joe Leibherr and put me on the phone with him.  Joe and Connie own the lot in Quartzite where we plan to spend part of the winter and I had a few questions for him.  (Dale and Sherry Leibherr bought most of Butch and Fonda’s business assets.  Dale is Joe and Connie’s son.)  I had a nice long chat with Joe and was satisfied that it will be an OK place to spend part of the winter.  Besides the full hookup 50A sites there is a laundry on site and Wi-Fi.  Verizon cellular service is also apparently very good.  Joe filled me in on some of things to do in town and suggested we bring our passports and visit Los Algodones, Mexico while we are in the area.  Brittiny and Rock stayed until 11:30 PM so it was a nice, long visit.  We were all really tired by the time they left and immediately turned in for the night.

2014/10/17 (F) VDO Air Power

After Brittani and Sterling (Rock) left last night I retired to the guest bedroom immediately but was up for a couple of hours responding to e-mails and writing my daily blog entry.  I do not shut my computer down every night but I do shut it down occasionally, especially if there are updates available.  Last night there were 28 updates.  I was not up at the crack of dawn today, which was a shame as it was the nicest weather day we’ve had for the week just past and looks to be the nicest of the week ahead.  Butch was up late last night as well, so we were both dragging a bit this morning.

Following breakfast I readied the coach for travel, securing loose objects inside and checking that all of the bays were shut tight and locked.  I switched on the chassis batteries and air valves, unplugged the shorepower cord, and went for a short test drive to calibrate our new VDO electronic speedometer.  Butch mentioned that there was a funeral home on the northwest corner of SR-16 and US-31 where he had easily turned their bus around in the past.  That turned out to be just what I needed for my test run as it kept me from having to go south on US-31 in order to make a U-turn to get headed back to Twelve Mile.

I had driven the coach last Sunday from Elkhart to Twelve Mile with the new speedometer set to its default pulses per mile and it indicated less than 1/8th of the actual speed as shown on our Rand-McNally 7710 RVND GPS.  When I got to Twelve Mile I calculated the pulses per mile I thought would be close to correct and programmed that number into the instrument.  On the first leg of my test drive this morning the indicated speed was still about 1/8th of actual.  Either my programming did not “stick” or I based my calculation on a grossly inaccurate assumption.

I pulled into the far entrance to the funeral home parking lot and made a broad turn to get lined up with the other entrance.  I switched off the ignition, held down the button on the face of the VDO, turned the ignition back on, and started the engine.  The speedometer cycled through its three calibration modes and I stopped it on ADJUST and then selected UP as the direction the needle needed to move.  The adjustment was a little tricky, especially while driving, but I figured out how to switch it between up and down.  I got it adjusted to my satisfaction before getting back to Twelve Mile and after not adjusting it for a minute or so it reset and reverted to its standard speedometer/odometer display, only this time showing the correct speed and recording the correct mileage.

When I got back to Butch and Fonda’s house I pulled the bus around, blocking the street temporarily, and backed it in next to theirs.  Fonda helped spot me for the final few feet.  Instead of shutting the engine off I let it idle while I got my four chassis stands out of the warehouse and positioned them at the four corners of the bus.  I put the engine in high idle and raised the body as high above the axles as it would go.  I slid the stands into place under four frame members, dropped the idle to low, and gently lowered the bus until it was resting firmly on the stands.  With the bus sitting on the stands it will now be safe to work underneath it when we get around to those projects.

The next project was to replace the air filter / water separator for our auxiliary air system.  Butch did most of the work on this project.  He disconnected two air lines from the existing filter assembly, which includes a pressure regulator and a Schrader valve, and then unscrewed the mounting bracket from the rear wall of the bay under the driver’s seat where a lot of the auxiliary air system is housed.

With the old unit out of the bus he was able to work in his shop to remove the inlet and outlet fittings and clean them up on a wire wheel before reusing them.  He installed the old fittings in the new housing using pipe thread compound and matched the alignment of the old unit so the air lines would fit back on to them.  The two machine screws that were used to mount the old unit’s mounting bracket to the wall were too big for the slots in the new unit’s mounting bracket so Butch used his Bridgeport vertical mill to slightly enlarge the upper slots.

With the shop work done I took everything back out to the bus and installed it, which consisted of attaching the two air lines (with compression fittings), attaching the mounting bracket to the housing, attaching the mounting bracket to the rear wall of the compartment, and then tightening the two air line nuts.  Butch checked my work and snugged the air line nuts another partial turn.

I turned on the auxiliary air compressor but it seemed to take a long time to start to build air pressure and Butch heard and felt a leak at the unloader valve coming out of the auxiliary air compressor.  I shut of the aux compressor and he hooked up his portable air compressor to the air hose fitting in the passenger side engine bay which brought the pressure up in the auxiliary system very nicely.  We turned his compressor off, turned the aux compressor back on, and bled enough air off to cause the aux compressor to run.  It finished bringing the pressure up to the cutout value without difficulty.  I sprayed all of the fittings with Simple Green and did not detect any leaks.  We had noticed earlier that the lower half of the filter housing, which locks and unlocks in only 1/8th of a turn, had a loose fit.  Once the system was pressurized, however, it tightened up.

Norgren auxiliary air filter / water separator (lower right).

Norgren auxiliary air filter / water separator (lower right).

The old unit had to be replaced because it was no longer made and the replaceable filters were no longer available.  Once we had it out of the coach and disassembled I was surprised by how badly deteriorated it was internally.  Aluminum, by definition, does not “rust” but it certainly can and does corrode (oxidize).

Butch and Fonda spent part of the day building and installing a slide out tray for one of the passenger side bays.  It will hold his tool box on top and have room for miscellaneous storage underneath.

I got the Zena power generating module wiring diagrams for Butch to study while I ate lunch.  We were just getting ready to start working on this when Jaral showed up.  He and Butch and Fonda talked for quite a while about personal stuff while I started probing around in the driver side rear electrical bay for a place to tap into an ignition switched source of 24VDC power.  I located a relay that looked like it would do the trick (R53).  I broke off working on this to spend time with Jaral, who rode his scooter from Logansport to discuss some cabinetry project.

Jaral looked at Butch’s projects first as they are immediate.  He then looked at what we want to do with the front part of our coach.  We need to have a desk and a printer cabinet built out of walnut to match the woodwork that is already in the bus and Jaral is our cabinetmaker of choice.  It sounds simple enough, but the reality is more complex.  After talking it through with him (again) and taking some measurements we agreed that I need to make very careful dimensioned drawings of exactly what we need.  I may try to do that over the winter but worst case is that it will have to wait until next spring and probably after we have removed the current furniture.

Butch and I worked on the Zena wiring for a little while after Jaral left.  We determined that the two blue wires in the electrical bay ran to the Zena control modules in the engine bay and to the fan terminals on the Zena rectifier assembly in the house electrical bay.  He had a tandem spade lug adapter that we used to tap into the power to the coil of relay 53.  With the coach batteries on but the ignition off we did not have power to the fans on the rectifier assembly or the control modules in the engine bay but with the ignition on we did.  That was a small but important success.

The weather had turned cloudy, windy, and chilly as the afternoon progressed.  We spent a little while studying my house electrical bay and discussing how I might get the large battery charging cables from the ceiling-mounted rectifier to a Class T fuse and then to the batteries.  I decided that was a problem I was not going to solve in the remaining hour of daylight and called it a day.  By then it was 6 PM so I went to my coach to have dinner which consisted of a salad, tofu hot dog, apple, and a glass of Franzia Moscato.  I retired to the guest bedroom around 9 PM, worked on my computer and iPad until about 10:30, and then turned off the lights.

2014/10/18 (S) Cold Wet & Windy

Even though I went to sleep at 10:30 last night I did not get out of bed until 8 AM this morning.  Today’s weather forecast was for a 50% chance of rain with winds out of the WNW shifting to N at 15+ MPH and a high temperature of 50 degrees F.  The 50% chance of precipitation turned out to be an all-day drizzle; not an ideal day for working outside.  Nonetheless, I spent the late morning (post breakfast) working in our house electrical bay on the wiring for the Zena 24 VDC power generating system.

The only thing I actually accomplished was mounting a Class T fuse holder (with a fuse) to the ceiling of the compartment.  That was a bigger accomplishment than it seems, however, as its location determined the lengths of the cables needed to finish the project.  With a nicer day on tap for tomorrow I expect to get those cables made and installed.  A final check of the wiring and installation of the drive belts on the alternator will complete the project, which I stated almost exactly two years ago.

20141018-09012

Zena rectifier (upper left) and Class T fuse (upper center).

 

Butch and I went to Logansport in the early afternoon.  He needed plumbing parts for his fresh water tank and ITR Oasis Combi project.  I needed 2/0 lugs for my battery cables, some 3/8 compression nuts and sleeves, and some duplex outlet expanders.  I found the lugs at Rural King (where we also got some free popcorn) and everything else at Home Depot.  These stores happen to be conveniently located across the street from one another.  The nuts and sleeves will be used to rig up a hose or tube so we can test the water flow coming out of the pipes that feed the kitchen faucet.  The flow is much lower than it should be and we want to determine if it is due to the faucet or upstream in the piping.  I found a small duplex to 6-out expander that would fit under the thermostat on the end of the kitchen counter based cabinet.  I also found a duplex to 6-outlet expander with integrated surge protection and two USB charging ports.  I bought two, one for the outlet on my side of the bed and one for the outlet on the outside wall just behind the passenger seat.  This model is not illuminated like the one I installed on Linda’s side of the bed, but that’s OK.

We stopped at Butch’s parents’ house to investigate the source of a mechanical noise. It turned out to be a dehumidifier in which the fan motor bearings were squealing.  Butch loaded it in his truck to take back to his house where he could more conveniently try to oil the bearings.  We chatted for a while and then headed to Martin’s Supermarket so I could pick up a few grocery items.

When we got back to Twelve Mile I unloaded and stored my groceries and then installed two of the three outlet expanders.  I could not install the one by the passenger seat as the outlet was too close to a wooden structure.  There is an outlet box with a solid cover plate next to the duplex outlet and I will see if the outlet can be moved over.  If not, I will install this unit behind Linda’s night stand at our sticks ‘n’ bricks house.

Butch’s brother, Tom, showed up and the two of them worked on installing the Blue Ox base plates on Butch’s Suburban.  I spent the afternoon making a scale drawing of the passenger side of the front half of the coach showing the two Lambright Comfort Chairs, custom printer cabinet/table, and custom desk with pantry.  I checked in with Butch and Tom and helped them a little bit with the base plate project.  When they reached a stopping point, or at least a point where my assistance was no longer needed, I returned to my coach and fixed dinner.

I had a salad of power greens with cranberries and peanuts, some apple sauce, and the leftover Mjadra from La Marsa, the last of my frozen leftovers from our dinner at the Brighton location with Bruce and Linda Whitney.  A glass of Franzia Moscato was quite agreeable.  Butch and Fonda had not eaten their dinner yet, so I worked in the guest bedroom at my computer while they ate.

Linda called around 8:45 PM and chatted with Butch about an accounting issue related to their business and then chatted with me about our grand-daughter, Madeline, who is finally pronouncing words clearly enough to be understood and quickly developing a spoken vocabulary.  Brendan and Shawna brought her to our house around 11:15 AM this morning and stuck around through lunch to get her down for her nap and then took off.  Grandma Linda had her all to herself the rest of the day and will have her tomorrow until they pick her up.  I chatted with Butch and Fonda for a while after that and then retired for the evening, checking and responding to a couple of e-mails, doing a little web-surfing, and working on this post.

2014/10/19 (N) Of Mice And Men

Although I really enjoy Linda’s homemade granola I decided to make toast with some of the Brownberry Country White bread I bought.  I was surprised to discover that someone, or something, had chewed a hole through the plastic bag and eaten some of my bread.  A mouse, no doubt, but I only bought this bread on Tuesday, so it was a recent visitor.  The surprise was that the bread was in a cabinet that I assumed was inaccessible to mice.

I emptied the cubby and discovered a hole in the back wall big enough to stick my finger through for some distance, which meant it was plenty big enough for a mouse to get through.  The walls are covered with the same thin carpet that is used to line all of the other cabinets in the coach.  In this case it was applied to fairly thin wood with space behind it.  Butch looked at it with me and we found that the glue used to install the carpet had lost much of its hold.  We lifted it up and found a 2″x2″ cutout in the wood with the hole in the carpet roughly centered on it.  There was a Romex electrical cable coiled up behind the wall with the ends taped.  We presumed the wire had once passed through the hole into the cubby but was now a way for the mouse to travel vertically through the cavity and get to the back entrance.

I threw the bread out, of course and cleaned the counter surface, which forms the floor of the cubby, with Lysol.  Mouse proofing the bread cubby will have to wait until tomorrow but my plan is to feed the wire through the hole in the carpet and then lift the carpet at the bottom and run a bead of caulk (or hot glue) along the joint between the counter and the wood walls.  I will then install a surface mounted outlet over the hole.  At a minimum it will seal the hole and it might prove useful someday for plugging in an appliance, assuming the wires are still energized.

Although it was in the low 30s when we got up this morning, it was finally a decent day for outside work.  The high temperature only made it to the mid-50s but it was sunny most of the day with a light breeze.  Appropriate layers of clothing made for comfort while working.

My main focus today was completing the installation of the Zena 24VDC power generating system in the bus.  I started this project two years ago this month and today was the day to finish it.  I had also written a complete draft of an article about this project for Bus Conversion Magazine but held off finishing and submitting it pending completion of the project.  Now that the work is completed and the system functions correctly I hope to finish the article in the next few weeks.

The purpose of the system is to charge/maintain the 24VDC house battery bank while we are driving the bus, during which time the refrigerator, and other minor loads, are being powered by the inverter.  The system consists of a high-output, continuous-duty, 24VAC, 3-phase alternator driven by the main bus engine (Detroit Diesel 8V92TA).  The alternator feeds a large rectifier assembly in the house electrical bay and is controlled by three interconnected modules mounted in the engine bay near the alternator.  Redundant voltage sense wires run from the rectifier back to two of the three control modules.  The system is activated by ignition switched 24VDC power which we wired up a couple of days ago.

The unfinished part of the project involved the connections between the DC output of the rectifier and the 24VDC house battery bank.  I mounted a Class T fuse on the ceiling of the electrical bay yesterday which then allowed me to determine several cable lengths.  On the +24VDC side I made three cables from 2/0 welding cable as follows:  1) Rectifier DC positive to ceiling fuse terminal A; 2) Inverter/charger fuse terminal B to ceiling fuse terminal B, and; 3) Ceiling fuse terminal B to +24VDC battery disconnect switch.  With this configuration both the rectifier and inverter outputs go through separate fuses to a common point (ceiling fuse terminal B) and that point is connected to the battery disconnect switch.  I also made a cable to go from the rectifier DC negative (ground) to the house DC electrical system ground lug; again using 2/0 welding cable.

I used a metal blade hacksaw to cut the welding cable to length and cut through the heavy rubber sheath 1/2 inch from the end to expose the copper conductors.  I attached crimp style through-hole terminals to the ends of the cables and held them in position to get the alignment correct.  I made reference marks to ensure the alignment and then crimped the lugs onto the wire using a very large hand-operated press in Butch’s shop.  Projects like this are a lot more fun with access to the correct tools.

I attached as many cable ends as I could without touching any live voltages.  I turned off the Aqua-Hot, the UPS, and the inverter/charger before disconnecting the main AC shore power.  I then turned the +24VDC disconnect switch to the off position, isolating the coach/inverter from the 24VDC battery bank.  (Note, however, that I did not disconnect the 12VDC center tap.)  With power off I completed all of the needed connections, including the small ground wire for the 24VDC fan on the rectifier, turned the 24VDC batter disconnect switch to ‘on’, and turned the inverter back on.  It immediately started supplying power so I knew my wiring was correct.

Back in the engine bay I checked all of the wiring against my diagram and everything was good to go.  I taped off two wires with bullet connectors on the ends to prevent accidental shorting.  One of the wires is used to reset the system by grounding it and the other wire is tied to chassis ground.  With all of the electrical connections verified I got Butch to help install the two drive belts from the DD8V92TA pulley to the alternator (power generating module).  That was when we discovered that the lower side of the belts were in contact with a pressurized oil hose for the Spinner II centrifugal by-pass oil cleaner.

The hose was secured with zip ties in several places so I clipped and removed those.  I disconnected the hose from the Spinner II and re-routed it to avoid the drive belts and other rotating parts on the front of the engine (which faces the rear of the bus).  I reattached the oil hose to the Spinner II and secured it with zip ties.

Butch used a pry bar to move the alternator and put tension on the drive belts while Tom and I tightened the alternator mounting bolts.  The inverter had been supplying AC power to the coach for a while and a check of the house battery voltage showed +24.5VDC.  I turned on the chassis batteries and engine accessories air valve, started the DD8V92TA, and put it in high idle.  I re-checked the voltage at the rectifier output and it was 24.8, higher than before and rising, but not too high; an excellent set point at least for now.

DD8V92TA with Zena 3-phase alternator lower right.

DD8V92TA with Zena 3-phase alternator lower right.

We observed that some of the belts on the engine seemed loose and floppy.  Butch also noticed what appeared to be a stone embedded in the outside surface of the Gates Hi-Power II PowerBand A92 triple V drive belt that runs from the DD8V92TA crankshaft pulley to the drive pulley for the engine cooling fan.  Butch called O’Reilly’s in Logansport but they were unable to locate the 2.125″ wide triple-V belt in their system.

The oil dipstick tube was also too close to the new drive belts but when I tied to move it (bend it slightly) I noticed that it was very loose.  The fitting at the block was not tight and it was obvious that some oil had leaked out from there.  I slid under the engine from the rear of the bus and tightened it at the block.  (It is nice having the bus supported on stands so I can work under it without concern.)

While I was working on the Zena system Butch installed an outlet fitting on their fresh water tank.  He and Fonda, and eventually Tom (Butch’s brother), re-installed the tank in their bus and then mounted the ITR Oasis Combi next to it, securing it to the floor of the bay.  To accomplish that they had to drill holes, align holes, and determine a location for the water pump, which required more information regarding allowable pump orientation.  Sometime during the day Butch shifted his focus towards an antenna project on the roof of their bus.  He had previously purchased a Tarheel motorized fold-over mount for his large Tarheel screwdriver antenna and wanted to at least get the fold-over mount attached to the roof before they left for the southwest.

The key lock on our passenger side engine bay door was getting difficult to turn so I removed an access panel on the inside of the bay door to investigate the mechanism.  As I loosened the access panel water ran out the bottom.  We determined that the gasket surrounding the handle/lock assembly was dried out and cracked, allowing water in at the top.  I removed the handle/lock assembly by pulling it out of the door from the outside, dried it out, and lubricated it.  I reassembled it for now, but I need to apply some kind of sealant behind the gaskets or get new ones from Prevost (if they are still available).

Prevost H3-40 keyed, non-electric, door lock mechanism.

Prevost H3-40 keyed, non-electric, door lock mechanism.

Butch shifted his attention yet again, this time to their Suburban where he and Tom re-attached the front bumper.  It was removed a few days ago so he and Tom could install the Blue Ox base plate kit which will allow them to tow it with the bus.

As the sun dropped low in the western sky the temperature dropped along with it.  I buttoned up my coach and helped Butch get his tools and supplies moved inside.  I then went to my coach to have dinner which consisted of an Annie’s Spicy Mongolian noodle bowl with added peanuts and a tofu hotdog with mustard, onion, and relish.  A glass of Moscato with the meal and a cup of Oriental Treasure green tea afterwards provided a soothing and warming end to the meal.  I returned to the house and we chatted for a short while before I retired to my room to check e-mail and write.

2014/10/20 (M) Bad Timing

I have settled into something of routine on this extended visit to Twelve Mile, Indiana; up late, sleep late, eat breakfast, get to work.  Usually.  Butch spends the early morning on his computer and is usually ready to work about the same time I am.  Usually, but not always.  Sometimes he gets to work earlier than me, and sometimes much later.  Although we had a beautiful weather day (except for the brief thunderstorm around 10 AM) we were not able to take full advantage of it for various reasons.  I had left the Aqua-Hot turned off over night to see if it would start reliably when cold.  The burner fired after a short 10 second purge.  It was smokey at first, but ran its full cycle and eventually cleared up.  I turned it off and will test its cold start capabilities again tomorrow morning.

We discovered yesterday that the triple V fan belt on my bus engine was worn and had something embedded in it.  The belt was a Gates Hi-Power II PowerBand A92.  We spent some time looking for one online but were not sure we had found exactly the right one so I decided to see if Prevost had it in stock.  They did, and it was only a few dollars more, included free shipping (as always), and would be at my house before I got home.  I ordered two.  This belt drives the engine cooling fan and if it breaks the bus isn’t going anywhere until it is replaced.

Bread cubby with AC outlet base plate.

Bread cubby with AC outlet base plate.

Butch and Fonda worked on re-conditioning a pair of fan-coil heat exchangers that will get tied-in to their new ITR Oasis Combi hydronic heating system on the bus.  Butch and I had both been assembling shopping lists and I was at the point where I needed to get some small parts in order to move forward with some small projects.  We left around 11:30 AM and drove to Logansport where we visited NAPA, O’Reilly’s, Rural King, Aldi’s, Home Depot, and Walmart.  All of these stores are located close to one another on the east end of town except for the O’Reilly’s and NAPA which are just a bit farther down the main road towards downtown.  When it comes down to it, Logansport is just not that big.

By the time we got back it was after 3 PM and we were suddenly very busy as we tried to take advantage of the few remaining hours of daylight.  Butch and Fonda worked on installing the Tarheel fold-over mount and I worked on sealing the bread cubby, installing a Wiremold surface mount outlet over the hole in the back wall, and installing a small battery powered LED puck light in the back closet to illuminate the inverter sub-panel.  I cut a small triangle of thin aluminum for the hole in the corner floor of the bread cabinet and then sealed the joint between the floor (counter) and three walls with a silicone-based paintable tub and tile caulk in a convenient squeeze tube.

LED puck light in rear bedroom closet to illuminate the inverter sub-panel.

LED puck light in rear bedroom closet to illuminate the inverter sub-panel.

When I finished those tasks I checked in with Butch and Fonda and found out that they had run into problems with the Toggler(R) bolts Butch was using and had to undo what they had already done and seal up the holes in the roof for the night.  There wasn’t anything I could do to help at that point, so I started working on the wiring that will allow me to relocate the Magnum ME-ARC remote control/display module from the electrical bay to the house panel next to the refrigerator.  Rather than try to route the 4-wire telephone cable between the inverter/charger and the house panel, John Palmer had suggested two years ago that I re-purpose one of the existing cables that had previously connected the Heart Interface inverter/chargers to their remote displays.  All that was required was to attach RJ-11 plugs on each end to four off the nine available wires.  As long as I used the same four wires on each end, and got the colors in the same order, it should work fine.  Butch already had the necessary crimper and I bought a small bag of the plugs today at Home Depot.

Sunset is just before 7 PM these days.  It not only comes earlier, it comes quickly.  We were done working by 6:30 PM and I withdrew to my coach to have dinner.  I had a nice salad of power greens with sun-dried tomatoes, olives, garlic, artichoke hearts, dried cranberries, and peanuts with peanut butter and crackers on the side and a small glass of Franzia Moscato.  I cleaned up from dinner, closed up the coach, set the two small electric cube heaters for around 60 degrees F, gathered up a few things and went back to the house for the evening.  Butch and Fonda were just getting ready to eat their dinner so I retired to my room to work on my computer.

2014/10/21 (T) Fair Weather Ahead

One of the first things I do each morning, even before I have breakfast, is to check the current and forecasted weather.  The guest bedroom at Butch and Fonda’s place is an interior room with no windows and is well insulated, including the ceiling, so I have no visual or auditory reference to what is happening outside.  If not for the clock on the headboard of the bed (or my various communications and computing technologies) I would have no idea what time it was, or even if it was day or night.

There was widely scattered light rain across northern Indiana at 7:30 AM with single digit precipitation probabilities through the day dropping to zero chance of rain for Wednesday and Thursday with high temperatures in the mid-to-upper 50s.  That is about as good as it gets for the fourth week in October.  Hopefully it bodes well for our project work and will be a very productive few days.

Butch plans to attend a gun show on Saturday morning and needs to spend most of Friday getting ready.  Butch and Fonda’s family members (parents, siblings, children, etc.) are gathering at their house on Sunday to celebrate the holidays early since Butch and Fonda plan to be in the southwest with us this winter.  Given the weather forecast I will probably work the whole day on Thursday, spend the night, and then head for home early Friday morning, or at least as early as I can manage.

Butch’s main focus today was re-mounting his Tarheel antenna lift to the roof of their bus.  He figured out last night what parts he needed to make the installation work after his Togglers(R) broke yesterday.

My main focus was diagnosing and repairing the very low water flow from the kitchen faucet but before I got too deep into that project I called Prevost’s U. S. parts office in Elgin, Illinois to check on a couple of things.  They had the CX-96 cogged fan belts in stock in the U. S. but wanted $90 for a pair (they only sell them in pairs).  I found them last night online for $21 each, so that was a big difference.   They also had the bay door handle/lockset gaskets I needed but they were only stocked in Canada.  They were only $4 each, so I ordered the 12 I need to redo every door.

The disassembled kitchen faucet flow restrictor.

The disassembled kitchen faucet flow restrictor.

I found the installation and instruction manual for the Kohler kitchen faucet in our conversion binder.  It said that the handle and cover should slide straight off of the body once the handle set screw was removed.  Butch and I both tried this but we could not get it off.  While studying the diagram and parts list I noticed a “restrictor” that also served as an adapter from the 8mm outlet pipe on the faucet to the 1/2″ NPT fitting on the retractable hose assembly.  At Butch’s suggestion I shut off the bus fresh water pump, shut the valves on both the hot and cold supply lines that feed the kitchen sink faucet, and disconnected the supply lines from the inlet tubes that are part of the Kohler faucet.  I inserted the barbed end of the 1/2″ NPT adapter into a piece of rubber hose that I got from Butch and threaded the pipe thread into the cold supply line.  I placed the end of the hose in a bucket, turned on the pump, and then opened the cold supply valve.  I had lots of flow.  I closed the valve, shut off the pump, and repeated this for the hot supply which also had good flow.  That meant the problem was either in the restrictor, in the valve cartridge, or somewhere in the faucet body.  The good news was that the restriction was not in the upstream plumbing.

By mid-morning Butch was ready to make a parts run so I grabbed my short shopping list and rode into Logansport with him.  When we got back I disconnected the kitchen faucet hose from the restrictor/adapter and then disconnected the restrictor/adapter from the 8mm outlet tube.   The garbage disposal was in my way so I disconnected and removed it temporarily.  Initial inspection revealed that the restrictor was clogged so I started taking it apart and Butch finished the disassembly.  I reinstalled the adapter without the restrictor parts and tested the flow.  It was now very strong, which meant that the valve cartridge and valve body were OK and did not need to be serviced or replaced.  That was a good thing as we had not been able to remove the cartridge earlier when we tried.  With the water shut off I removed the flow restrictor/adapter cleaned out the entire assembly, and removed one small rubber O-ring.  I reassembled all of the pieces, turned the water on, and checked for leaks.  I did not see any so I turned off the water and cleaned up the area.

The Tarheel roof mount antenna lifter.

The Tarheel roof mount antenna lifter.

It was early afternoon by the time I finished the faucet project—too early to stop working on such a perfect weather day—so I started working on the wiring for the Magnum ME-ARC remote, which I want to relocate from the electrical bay to the house panel in the kitchen.  Because of the difficulty of running wires between these two locations I decided to follow John Palmer’s advice and re-purpose one of the two nine-conductor serial cables that connected the old Heart Interface EMS-2800 inverter/chargers to their remote panels in the house panel.

I decided to use the cable labeled #2.  I removed the snap-together Amphenol DB-9 connector from the house panel end and cut the molded DB-9 connector off of the inverter end.  I tried using Butch’s RJ-11 strip/crimp tool and discovered that the wire in the cable was one size too large to fit in the stripper so I stripped and trimmed them by hand.  The wires were stranded so I twisted them tightly but found that I could not get them inserted and lined up properly in the RJ-11 connectors I bought at Home Depot the other day.  Ugh.  Time for Plan B.

While we were working today plans got made for dinner at the Hibachi Grill Supreme Buffet in Kokomo, Indiana at 6:30 PM.  I decided to drive myself and leave early enough to go to Discount Tire in Kokomo and have them balance all four of my tires.  They closed at 6 PM so I stopped working around 3:30 PM, changed into cleaner clothes and headed for Kokomo at 4:15 PM.  Kokomo is about 30 miles south of Twelve Mile and takes about 45 minutes with speed limits and stop lights.  It used to be on US-31 but Indiana has made significant changes (improvements) to US-31 so that it is now a four lane divided limited access highway in many places and bypasses a lot of towns, including Kokomo.  What was US-31 is now SR-931.  Why they named it that instead of “Old US-31” as they have done in other spots is a mystery to me.

Before I got to Discount Tire I passed a Gordon Food Service (GFS) and a Menard’s located next to one another.  I needed things from both but wanted to get the car taken care of first.  Discount tire said it might be 90 to 105 minutes before they could get to me.  I could not wait that long but had them write it up anyway.  They took my car in about 25 minutes later and had it done in another 15 minutes, so I had time to do some quick shopping.

I got a package of 25 16 oz. hot cups at GFS to go with the lids we already had.  At Menard’s I got two surface mount 4-wire phone jacks and a double-ended phone cord for my Magnum inverter/remote project.  Butch and Fonda also stopped at Menard’s looking for dryer vents to use with their bathroom and shower ventilation fans.

Dinner at the Hibachi Grill Supreme Buffet was a family gathering.  Beside Butch and Fonda (and me) we had Butch’s mom and dad, his sister Robin and her mother-in-law Betty, Butch’s brother Tom and his wife Tracey, their son Brock and his wife, and another young couple and their kids.  I think the wife was Tom and Tracey’s daughter.  There were four or five kids whose names I did not get.  We all ate too much.  The food was OK, but Butch’s family and the conversation were more interesting.  It was 9 PM by the time we got back to Twelve Mile and I headed off to bed to take care of correspondence and writing.

2014/10/22 (W) Plan B

You always need to have a “Plan B,” or be prepared to come up with one on short notice.  Backup plans are not a sign of indecision or a lack of commitment to a primary plan.  Rather, they are an acknowledgement of the reality that things do not always work the way you thought they would no matter how brilliantly conceived, carefully planned, and skillfully executed.  So it was with my inverter/remote re-wiring project.

I spent most of the day working on the wiring that would allow me to move the Magnum ME-ARC remote from the electrical bay, where it was plugged directly into the Magnum MS4024 inverter/charger, to the house systems monitoring and control panel next to the refrigerator.  It was simple enough in concept, but I had to make sure it was correct as I did not want to damage the inverter or the remote unit.

I used four of the nine wires in one of the old serial cables (#2) that runs from the electrical bay to the house panel.  Since the phone line cables with the RJ-11 plugs on the ends used Black, Red, Green, and Yellow I decided to stick with those colors all the way through.  However, because of the way the RJ-11 connectors are assembled onto the cable the signals move back and forth between pins.  I ended up wiring the cable end in the electrical bay to the same color wires in the baseboard outlet and mounted it to the ceiling of the bay.  I cross-wired the other end of the cable to another baseboard outlet and mounted it to the side of the cavity behind the house system panel.  Fortunately the back side of the panel is accessible via a removable panel in the back of the closet that is on the other side of that wall.

With all of the wiring done I used a jumper with alligator clips on each end to bridge two of the wires in the electrical bay outlet and do a continuity check at the house panel outlet to verify the wiring.  Everything looked good so I unplugged the remote, brought it inside, and plugged it in.  It worked!  Now all I had to do was mount it.

There were already two cutouts at the bottom of the house systems panel from the old Heart Interface EMS-2800 remotes (the coach had two of these inverter/chargers when we bought it and each one had its own remote).  The cutouts measured 4.625″ W by 2.875″ H.  The housing on the ME-ARC was slightly wider than the opening but not as high.  Depth was not an issue.  I borrowed a small roto-tool from Butch with a small router bit and carefully opened up the left hand edge of the right hand cutout.  Using the remote as a template I marked the locations for the four corner screws, moved the remote out of the way, drilled out the holes, moved the remote back into position and attached it to the house panel using four #6 machine screws and Nylok nuts that I got from Butch.

The house systems panel with Magnum ME-ARC remote installed at lower right.

The house systems panel with Magnum ME-ARC remote installed at lower right.

While I was working on my project, I periodically asked Butch if he needed any assistance, but Fonda was providing the needed help.  They managed to mount an 18″ H by 24″ long piece of 3/4″ plywood to the back wall of the Oasis/water bay with a 1/4” heavy rubber separator between the wood and the metal.  Butch then mounted their Shur-Flo 4048 water pump to the plywood.  This should cut down considerably the noise and vibration transmitted from the pump to the structure of the bus and into the living quarters, but only experience will prove if that is the case.  Butch moved their fresh water tank slightly to make room for their portable water softener.  They also installed the two dryer vents, one on each side of their bus, which they picked up at Menard’s last night.  Their final project for the day was to cut a hole in the roof and install a right angle cable junction box that will be used to route coaxial cable and other lines from the roof into the passenger-side cabinet in the bedroom at the rear of their bus.

I looked at installing the remote readout for our Progressive Industries EMS-50 and decided it was more work than I wanted to start late in the day.  Butch suggested that I do it the same way I did the Magnum remote, re-purposing some of the wires in the old serial data cables.  That was going to require additional parts, so I started a list for my next trip to town.

My final project for the day was to try and fix the lighted entrance handle and the non-functioning patio light.  The lighted entrance handle had a badly deteriorated gasket behind the top securement so I fashioned a replacement from a piece of heavy vinyl shower pan liner that Butch and Fonda had.  The bulb was an LED I installed some time back.  It was still working but the socket was loose so I tried to squeeze it down a bit.  Butch pushed the spring loaded center section out, stretched the spring, and put it back in.  The bulb is now nice and tight.

The patio light proved to be more difficult.  The lens was cracked and difficult to get out but I finally did.  It’s a florescent fixture with two F8T5 bulbs.  I tried turning them in their lampholders but that did not help.  I pulled the wires far enough out of the wall to find two butt connectors.  I was able to get my multimeter probes far enough into one end of each connector to verify the presence of 13 VDC that was controlled by the same switch as the lighted door handle.  I removed the two bulbs and tested them in the fixture over the kitchen sink.  They both worked fine, so the problem appeared to be the ballast.

The way the fixture is designed there was no way to get to the ballast to replace it so I put the bulbs back in and got them to glow faintly.  I tried to replace the lens, which was already cracked, and the top inch split off all the way across.  Fonda though she could fix the cover and epoxied the two pieces back together.  While the epoxy was setting up I noticed that both lamps had come on full bright.  By the time Butch reinstalled the lens they had both gone out.  Definitely a bad ballast.

As it turned out, Butch had an almost identical brand new fixture that he did not intend to use.  The only difference was that his fixture had an on/off button on the underside whereas the one on our coach has a plastic plug in that hole.  His fixture has black end caps, which is fine, and is not painted to match the color of our coach, which is also fine.  Removing our current light fixture will be a bit of project and will have to wait until next week.

I ended up going to Logansport at 7:15 PM for a few parts that I would need tomorrow.  I got back around 8:30 PM and it took me 20 minutes to get my dinner ready and take it into the house.  I was straightening up the bus after dinner and looking for a new roll of paper towels for the kitchen when I discovered a mouse nest in the small cabinet between the sleeper/sofa and the kitchen base cabinets.  I put on nitrile gloves and cleaned it up and then inspected the compartment.  It was open at the back to the area above the HVAC chase that is part of the bus.  The more I have peaked in and under cabinets the more I have come to realize that our coach is a lot like Disney World; there is a network of passageways that are hidden from view but interconnect the bays with the areas behind and under cabinets and furniture, providing an subterranean road system for small critters.  It’s always something when it comes to bus conversions.  The long term challenge will be to figure how where the critters are getting in and see if we can plug those ports of entry.

 

2013_09_20 (Fri) Techs and Trains

The Frustrated Maestros perform each day at breakfast.

The Frustrated Maestros perform each day at breakfast.

I was up early again working on blog posts and finally uploaded several pertaining to early last week.  By the time Linda got up it was time to walk over and get some coffee.  We tried to catch Michael Canode before his 9:00 AM seminar on digital photograph, but did not get there in time.  I missed his seminar yesterday on designing and publishing website, but he offered to bring a copy of the handouts to today’s seminar.

Breakfast was coffee and donuts (rear) with “concert” and table seating.

Breakfast was coffee and donuts (rear) with “concert” and table seating.

We headed back to the vendor area, found Lloyd De Gerald, and paid him for the annual maintenance he did on our Aqua-Hot yesterday.  We also bought a replacement nozzle to keep on hand.  Lloyd suggested that we have the spare nozzle installed at our next annual service and buy another one to replace it at that time.  His experience has been that nozzles that sit unused for too long often do work well when they are finally installed.

The morning was overcast and a bit dreary, so there were not a lot of folks talking to the outside vendors.  We took the opportunity to chat with Lloyd about our interior remodeling plans and asked him what issues we should anticipate in moving the heat exchangers.  He said that the coolant loops can be difficult to prime if they get drained and suggested that once we had re-plumbed everything it might be best for us to have him refill and start the system.

He also indicated that we could have up to three heat exchangers on each of the three zones (bedroom, bathroom, and living room / kitchen.)  We have one heat exchanger in the bedroom, one in the bathroom, and two in the living room.  We also have radiators in the water bay and the front storage bay.  Lloyd indicated that the water bay was probably plumbed in with the bathroom and the front bay was probably plumbed in with the LR/kitchen, but that was not guaranteed.  It should be easy enough to determine this by turning on the Aqua-Hot and then activating one zone at a time and checking for heat; I just haven’t bothered to do this yet.  He suggested that we add heat exchangers to have three per loop, and that we replace the radiators in the bays with heat exchangers (which have fans).  He also said the newer heat exchangers are smaller and much quieter than the ones that are probably in our bus conversion, and that we should probably replace those as well when we remodel the passenger side of the kitchen/LR area.

We needed to kill some time before Michael’s seminar ended, so we strolled through the inside vendor building again.  The FMCA booth had shirts on sale, and they were even cheaper with our “rally bucks” coupons, so we bought a matching pair of plum pocket Ts.  (The matching clothes phenomenon gets a double whammy due to age and RVing sub-culture.)  We caught up with Michael at the end of his photography seminar.  Someone had taken the handout he brought so he e-mailed the PowerPoint file to me.  We ran into Butch and Fonda.  Butch and I decided to wander over to Ron & Meredith Walker’s coach to see if we could fix the new door latch.  The part arrived yesterday from Prevost and Ron had installed it, but it wasn’t working quite right.  Butch saw what was wrong right away and corrected it.  We then returned to our buses where Linda and I had leftover pizza for lunch and I took a nap.  (That’s the problem with getting up really, really early; not that I consider taking a nap a problem.)

The Blue Ox technician showed up mid-afternoon to service our Avanti II tow bar and brought my nap to an end.  The tow bar is showing signs of stretching in the latch pin holes and will apparently need to be replaced sooner rather than later; but not today.  He completely disassembled the tow bar, cleaned it thoroughly, added new rub plates (washer), lubricated it, and reassembled it.  I thought that was a pretty good deal for $25.  Since I was now awake again, I did more work on blog postings and we had more leftover pizza for dinner.

I have been remiss in not saying more about the trains going past the fairgrounds. The trains have been so constant here that I am hardly aware of them anymore and keep forgetting to mention them.  The tracks run along the southern edge of the fairgrounds and the trains seem to be almost constant at times.  Linda read online that a train passes through Goshen approximately every 6 minutes, presumably headed to or from the Chicago area to points east and south of here.  These are often medium length trains traveling fairly fast in both directions and the sound their horns long and loud at every crossing, of which there appear to be a very large number.

Linda talking with Alma Baker (L) and George and Sue Myers (R) at the reception for officers and vendors.

Linda talking with Alma Baker (L) and George and Sue Myers (R) at the reception for officers and vendors.

We went to a 4:15 PM reception for officers and vendors.  This was a “ticketed” event, and we got to attend because Linda is the Treasurer of the Great Lakes Converted Coaches, which is organized under GLAMA, and I am the VP/Secretary of the Freethinkers Associate Chapter, which is organized under the International Area (INTO).  This was another new feature at this rally, and was another example of how FMCA and its area associations are trying to recognize those who serve and make FMCA function.

Officers reception in the food hall, hor d’oeuvres and beverages on the left, seating on the right.

Officers reception in the food hall, hor d’oeuvres and beverages on the left, seating on the right.

FMCA has 11 areas and almost 500 chapters, but many of the members do not belong to a chapter and/or have never been to a rally.  Not that chapters and rallies are for everyone, but FMCA is very much aware that members who do not get involved in a chapter and/or attend an occasional rally often do not remain long-term members.  And why should they?  If you don’t engage with the people that are the organization, the benefit of membership boils down to a monthly magazine.  This is essentially our relationship with the Good Sam Club up to this point.  Our Good Sam membership is paid through 2017, but I don’t know if we will renew it at that time.  We have, however, met several people over the last few months that recently attended Good Sam rallies and said they were excellent and that they had a great time.  Of course, endorsements are like movie reviews, not very meaningful unless/until you can calibrate your taste with that of the reviewer.

The last light of the day.

The last light of the day.

The reception provided enough food for our dinner and we returned to our coach to relax before going to the evening entertainment.  The last light of the day turned dramatic as we were preparing to leave.  The featured performer for the evening entertainment was Sarah Getto, assisted by her father, who drives her motorhome, sets up the equipment, and runs the sound board.  He is also a guitarist and adds guitar and vocals to some of her songs.  Blind from birth and born with a cleft palette and lip, she is now an attractive, talented, 29 year old singer/songwriter with a music education degree that included training as an opera singer  Her preferred vocal style, however, tends to lean towards country, although she does a very good impersonation of Karen Carpenter.  She has much richer sound on stage than you would expect from a solo keyboard, as she prerecords richly layered sound tracks and then performs along with them.  All of the vocal and instrumental work on these sound tracks is done by her, and her dad was very transparent about the process Sarah uses to create her shows.  We enjoyed her performance along with the rest of the audience.

The evening concluded with a 50/50 drawing and door prizes.  We didn’t win anything, but that was OK.